N3MG

Substantial
None

Beech S35 S/N: D-7856

Accident Details

Date
Tuesday, March 24, 1998
NTSB Number
SEA98LA052
Location
MEDFORD, OR
Event ID
20001211X09784
Coordinates
42.280651, -122.899932
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

the pilot's inadequate fuel management. Factors were the pilot's diverted attention and soft terrain in the forced landing area.

Aircraft Information

Registration
N3MG
Make
BEECH
Serial Number
D-7856
Engine Type
Reciprocating
Model / ICAO
S35 BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Analysis

On March 24, 1998, approximately 1302 Pacific standard time, a Beech S35, N3MG, lost engine power and was forced-landed approximately 1/4 mile short of the runway while on visual approach to runway 32 at Rogue Valley International-Medford Airport, Medford, Oregon. The airplane was substantially damaged in the forced landing, and the private pilot-in-command and two passengers (both children of the pilot) were not injured. The 14 CFR 91 flight departed Redlands, California (a straight-line distance of 565 nautical miles from Medford) at 0915. Visual meteorological conditions, with light rain, prevailed in the accident area, and the flight was on an instrument flight rules (IFR) flight plan.

The pilot reported that he departed Redlands with 74 gallons of fuel on board. An FAA on-scene investigator reported that at the accident site, the aircraft's left fuel tank contained 23 ounces of fuel, and the right tank contained 14 gallons of fuel. The FAA investigator reported that there was no evidence of a fuel leak or breached fuel tank at the accident site. The FAA investigator reported that he checked the airplane's electric fuel pump after the accident, and that it provided good fuel pressure.

In his accident report to the NTSB, the pilot stated that on final approach for runway 32, after being cleared to land by Medford Tower, the engine quit without any warning. He stated that he tried switching tanks, a throttle and mixture adjustment, and an engine restart, all without success; he then had only enough time to land the airplane. He performed a forced landing onto a small, soft, level field on airport property. In his NTSB accident report, the pilot acknowledged that the engine power loss was due to fuel starvation, and reported that no mechanical failure or malfunction was involved in the accident. He stated that at about the time he was to have switched to the right tank, he was occupied with donning oxygen on himself and his children, and that soon afterward, his daughter started not feeling well and complained of headaches. The pilot stated that his concern for his daughter distracted him from his other pilot duties. The engine power loss occurred about 45 minutes after this event.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA98LA052