N92997

Substantial
Minor

Commonwealth 185 S/N: 1731

Accident Details

Date
Sunday, June 28, 1998
NTSB Number
CHI98LA227
Location
OREGON, WI
Event ID
20001211X10273
Coordinates
42.919040, -89.380958
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the improper adjustment of the carburetor by an unqualified person. Factors to the accident were the annual inspection not being complied with and the lack of recent experience of the pilot.

Aircraft Information

Registration
Make
COMMONWEALTH
Serial Number
1731
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
185
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
185

Registered Owner (Current)

Name
BARGER ALBERT L
Address
6872 VALIANT DR
City
WINDSOR
State / Zip Code
WI 53598-9514
Country
United States

Analysis

On June 28, 1998, at 1430 central daylight time, a Commonwealth 185, NC92997, piloted by a student pilot, sustained substantial damage when it impacted the terrain during a forced landing following a loss of engine power during takeoff from runway 36 (2000' x 30', wet, grass) at a private airstrip near Oregon, Wisconsin. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The pilot reported minor injuries. The local flight was originating at the time of the accident.

In a Federal Aviation Administration (FAA) inspector's statement, the inspector stated that he had interviewed the pilot, subsequent to the accident, and the pilot stated that he had no recollection of the events surrounding the accident. The pilot had sustained, as a result of the accident, a closed head trauma just above his right eye and bridge of nose.

The FAA inspector stated, in his written statement, that the aircraft's engine lost power soon after takeoff from the private airstrip. The inspector stated that the aircraft was found 300 yards from the end of the airstrip.

Post accident investigation showed that the aircraft was using auto-gas. There was no Supplemental Type Certificate (STC) found to be issued by the FAA for the use of auto-gas in the above stated aircraft. Approximately 1/4 cup of oil was drained from the number two cylinder. The lower spark plug of the number two cylinder was oil fouled. The number one cylinder upper spark plug lead fell apart when removed from the cylinder. The right magneto did not produce a spark when a functional test was conducted. In a statement to a Dane County Sheriff's Office deputy, the pilot stated that on the day of the accident he had noticed that the carburetor of his aircraft was running "Over." The pilot stated that he readjusted the carburetor to specifications. According to a FAA inspector statement, the most recent annual inspection was completed on October 10, 1996.

The FAA inspector stated in a phone conversation, with the investigator-in-charge (IIC), that the last 90-day student solo sign off was in October of 1997. According to the pilot's written statement there was no record of flying for at least 90 days prior to the date of the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI98LA227