N96GF

Substantial
None

Fife LANCAIR 320 S/N: 633-320-378

Accident Details

Date
Monday, June 15, 1998
NTSB Number
LAX98LA204
Location
PALM SPRINGS, CA
Event ID
20001211X10360
Coordinates
33.849334, -116.559860
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A failure of the electrical system for undetermined reasons. The pilot's decision to continue flight with a suspected electrical system anomaly is a factor in the accident.

Aircraft Information

Registration
Make
FIFE
Serial Number
633-320-378
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
LANCAIR 320
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
LANCAIR 320

Registered Owner (Current)

Name
HILE PHILLIP J
Address
231 GEORGE LEWIS CT
City
HARRISON
State / Zip Code
OH 45030-4919
Country
United States

Analysis

On June 15, 1998, at 1300 hours Pacific daylight time, an amateur built experimental Fife Lancair 320, N96GF, landed with only the right main landing gear extended during a precautionary landing on runway 13L at the Palm Springs, California, airport. The aircraft, operated under 14 CFR Part 91, sustained substantial damage. The pilot/owner, the sole occupant, was not injured. Visual meteorological conditions existed for the personal flight that had originated from Albuquerque, New Mexico, the day of the accident. A refueling stop was made in Prescott, Arizona, at 1105 mountain standard time and the flight was scheduled to terminate at the Oceanside, California, airport. No flight plan was filed.

The pilot reported that after refueling in Prescott he was unable to start the engine, and had to obtain a jump-start from a ground power source. After takeoff, he noted that the autopilot was not working and the main 50-amp circuit breaker had tripped. The pilot stated that he reset the circuit breaker and the ammeter showed a positive charge. Approximately 30 minutes after takeoff, he noted that the "radio [was] weak, also noticed fuel transfer pump weak." The pilot stated that he shut off all electrical power except for the transfer pump. Approximately 45 minutes later he noted that the header tank was 1/3 full. The pilot stated that he looked for an alternate airport to make a precautionary landing. He circled over the airport and attempted to manually extend the landing gear but only the right main gear fully extended. He landed on runway 13L with no flaps and came to rest off of the runway.

A Federal Aviation Administration inspector from the Riverside, California, Flight Standards District Office reported that the pilot trucked the airplane back to Albuquerque, New Mexico, and it was not inspected.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX98LA204