N500GQ

Substantial
None

Reinhold REVOLUTION MINI 500 S/N: 404

Accident Details

Date
Monday, October 26, 1998
NTSB Number
MIA99LA017
Location
HICKORY, NC
Event ID
20001211X11313
Coordinates
35.770591, -81.329452
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The seizure of the rear piston in the cylinder barrel resulting in total loss of engine power and an autorotation which resulted in main rotor contact with the tail boom while touching down on unsuitable terrain.

Aircraft Information

Registration
N500GQ
Make
REINHOLD
Serial Number
404
Model / ICAO
REVOLUTION MINI 500

Registered Owner (Historical)

Name
GRAUER REINHOLD
Address
4740 MATTHEWS WEDDINGTON RD
Status
Deregistered
City
MATTHEWS
State / Zip Code
NC 28105-9319
Country
United States

Analysis

On October 26, 1998, about 1515 eastern standard time, a Reinhold Revolution Mini 500, N500GQ, registered to an individual, crashed while making a forced landing following loss of engine power near Hickory, North Carolina, while on a Title 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The helicopter received substantial damage and the airline transport-rated pilot was not injured. The flight originated from Hickory, North Carolina, the same day, about 1600.

The pilot stated that while in cruise flight at between 500-700 feet, the engine quit with no prior warning. He initiated an autorotation and made a left turn toward a clearing. Upon touchdown on uneven terrain, the main rotor hit the mechanical stop and then contacted the tailboom. The helicopter spun around to the left 180 degrees and came to rest on the back skids and engine muffler. The clear area he selected for the landing was overgrown with about 6 feet of vegetation.

Postcrash examination of the engine by the pilot showed the rear piston had seized in the barrel. The pilot stated to NTSB that this was the second time this has happened in this helicopter. The engine had accumulated about 46 flight hours since it was rebuilt after the previous piston seizure.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA99LA017