N565ML

Substantial
Minor

Cessna 175 S/N: 55420

Accident Details

Date
Wednesday, November 25, 1998
NTSB Number
ATL99LA023
Location
LOCUST GROVE, GA
Event ID
20001211X11369
Coordinates
33.340747, -84.099121
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Loss of engine power due to a gear train failure in the accessory gearbox for undetermined reasons. A factor was the rough and uneven terrain.

Aircraft Information

Registration
N565ML
Make
CESSNA
Serial Number
55420
Engine Type
Reciprocating
Model / ICAO
175 C175
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
LEVY B JOSEPH
Address
565 MALLARD LN
Status
Deregistered
City
LOCUST GROVE
State / Zip Code
GA 30248
Country
United States

Analysis

On November 25, 1998, about 1525 Eastern Standard Time, a Cessna 175, N565ML, collided with the ground in a cow pasture while attempting an emergency landing following an engine failure in Locust Grove, Georgia. The airplane was operated by the private pilot under the provisions of Title 14 CFR Part 91, and visual flight rules. Visual meteorological conditions prevailed and no flight plan was filed for the local flight. The pilot and sole occupant sustained minor injuries, and the airplane sustained substantial damage. Origination of the flight was Mallards Landing in Locust Grove, Georgia, at 1500.

According to the pilot, while flying at cruise, the engine lost power over a 10 to 15 second period. There was no sputtering or shaking associated with the loss of power. Lining up with the contours of the pasture, the pilot attempted an emergency landing. After touchdown the airplane nosed over inverted.

Examination of the engine disclosed a gear train failure in the accessory gearbox, which prevented the camshaft from actuating the valves, and allowed only one magneto drive to rotate when the propeller was turned. According to the FAA Inspector who examined the airplane, the engine was not disassembled for further examination. Review of the maintenance records found that the engine was last overhauled on December 6, 1984.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL99LA023