N466MF

Substantial
None

Aegerter, Simon VELOCITY 173E-RG S/N: DMO-326

Accident Details

Date
Tuesday, December 29, 1998
NTSB Number
LAX99LA060
Location
SAN DIEGO, CA
Event ID
20001211X11586
Coordinates
32.799972, -117.129508
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The pilot's inadequate modification to the control systems, which resulted in a restricted elevator control.

Aircraft Information

Registration
N466MF
Make
AEGERTER, SIMON
Serial Number
DMO-326
Year Built
1998
Model / ICAO
VELOCITY 173E-RG

Registered Owner (Historical)

Name
SIMON AIRCRAFT INC
Address
2717 SPRUCE CREEK BLVD
Status
Deregistered
City
DAYTONA BEACH
State / Zip Code
FL 32128-6921
Country
United States

Analysis

On December 29, 1998, at 1547 hours Pacific standard time, a Velocity 173E-RG, N466MF, veered off runway 28L on landing at Montgomery Field, San Diego, California, and collided with a parked Cessna 340, N6241X. The aircraft and the parked and unoccupied Cessna 340 sustained substantial damage. The private pilot and his two passengers were not injured. Visual meteorological conditions prevailed for the personal flight from Ryan Field in Tucson, Arizona, to Montgomery Field. This was the last leg of a cross-country flight, which originated the day before in Tampa, Florida. No flight plan was filed.

The pilot stated that he had experienced insufficient pitch control on landing at Tucson prior to the accident. He reported that he "found play in the elevator control," and was advised over the telephone by the aircraft designer, Velocity Inc., to add washers or spacers to the rear of the torque tube to remove the play. With the aid of a local pilot in Tucson, he added the washers and spacers to the rear of the torque tube.

The pilot further stated that upon attempting to flare, "the nose would not come up." The aircraft bounced, veered off the runway, skidded across a grass area, and collided tail first with the parked Cessna 340.

According to the pilot, "on January 2, 1999, several Velocity builders inspected the airplane and found that the front bearing of the aileron torque tube had come loose, thus preventing a full elevator down deflection."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA060