N2313L

Substantial
Minor

Beech C23 S/N: M139

Accident Details

Date
Thursday, December 31, 1998
NTSB Number
LAX99LA062
Location
FURNACE CREEK, CA
Event ID
20001211X11588
Coordinates
36.599418, -116.829559
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's inadequate preflight inspection when he failed to remove the gust lock from the flight controls.

Aircraft Information

Registration
N2313L
Make
BEECH
Serial Number
M139
Engine Type
Reciprocating
Model / ICAO
C23 BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
UNDERWOOD HAROLD W
Address
43729 HOME PLACE DR
Status
Deregistered
City
LANCASTER
State / Zip Code
CA 93536-5895
Country
United States

Analysis

On December 30, 1998, about 1630 hours Pacific standard time, a Beech C23, N2313L, sustained substantial damage when it collided with terrain during a takeoff overrun from the Furnace Creek, California, airport. The private pilot/owner and his passenger both received minor injuries. The aircraft departed Lancaster, California, at 1000 for the flight to Furnace Creek. The personal flight was conducted under the provisions of 14 CFR Part 91. After touring Death Valley National Park, the pilot/owner and his daughter were departing for Lancaster when the accident occurred. Visual meteorological conditions prevailed and no flight plan was filed.

The pilot stated he performed his preflight in the tie down area. There was no wind so he elected to use runway 15. After checking visually and with Unicom, the pilot proceeded to back taxi on the runway to the departure end since Furnace Creek has no taxiway. He lined up in position for takeoff to conduct his takeoff checklist. He stated he became concerned that he could not see approaching traffic while he was pointed in this direction and considered repositioning so that he could. He maintained this position but decided to forego pulling the written checklist from the glove compartment and did the checklist by memory. After completing his run-up and checks, he announced his departure on Unicom, added full power, and began the takeoff roll. He estimated rotation speed (65 mph) was reached approximately 2/3 of the way down the runway. As he started to pull on the control yoke, he realized the gust lock pin was still in the locked position. He felt that he could not abort the takeoff at this point without departing the end of the runway at a high rate of speed. He attempted to remove the gust lock, which required him to depress a button on the bottom of the pin while pulling down on the shaft. As he was struggling with the pin, the aircraft overran the runway. The nose gear dug into the dirt and was sheared off. He estimated the aircraft came to rest 30-50 yards past the end of the runway. The pilot turned off the magnetos and fuel. He noticed that the key was sheared off and that the throttle was pulled out and bent down sharply. Lying on the floor was the gust lock pin and a broken part of its neoprene housing. Fuel was flowing down the right wing as the pilot followed his daughter out of the aircraft.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA062