N1035J

Substantial
Minor

AERO COMMANDER 112 S/N: 35

Accident Details

Date
Wednesday, July 21, 1993
NTSB Number
ATL93LA131
Location
BROADWAY, NC
Event ID
20001211X12773
Coordinates
35.450466, -79.050132
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

WATER AND CONTAMINANTS IN THE AIRCRAFT FUEL SYSTEM, AND THE PILOT'S INADEQUATE PREFLIGHT OF THE AIRCRAFT. A FACTOR WAS THE ROUGH TERRAIN AT THE FORCED LANDING SITE.

Aircraft Information

Registration
N1035J
Make
AERO COMMANDER
Serial Number
35
Engine Type
Turbo-jet
Year Built
1973
Model / ICAO
112 VNOM
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CENTRAL AIR PARTS INC
Address
3185 WILLHOIT AIRPORT RD
Status
Deregistered
City
STAUNTON
State / Zip Code
IL 62088-4150
Country
United States

Analysis

On July 21, 1993, at about 1137 eastern daylight time, an Aero Commander 112, N1035J, nosed over during a forced landing at Broadway, North Carolina. The private pilot and one passenger had minor injuries. The aircraft was substantially damaged. The aircraft was owned and operated under 14 CFR Part 91 by the pilot. Visual meteorological conditions prevailed at the time, and no flight plan was filed for the personal flight to Atlanta, Georgia. The flight originated in Rocky Mount, North Carolina at about 1102.

The pilot reported the following: While established in cruise flight at 2,500 feet mean sea level (msl), the engine lost power and quit. Attempts to restart the engine were unsuccessful. He flew a no flap approach into a tobacco field. During the landing roll, the nose gear collapsed, and the aircraft nosed over.

An airframe and powerplants mechanic inspected the aircraft following the accident. The electric auxiliary fuel pump was operated, and a trace of water came out at the outlet port. The fuel sediment bowl and gascolator were full of rusty colored water. The gascolator screen was coated with a slimy, rust colored substance. The flexible hose from the auxiliary pump to the engine driven fuel pump contained a slight amount of water.

According to maintenance records, the last inspection on the aircraft was an annual inspection on July 1, 1992. At the time of the accident, the aircraft had been flown about 4 hours since this inspection. The aircraft had been flown about 42 hours since February of 1990.

The pilot did not comply with 49 CFR Part 830, requiring the completion of NTSB Form 6120.1/2 (Pilot/Operator Aircraft Accident Report).

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL93LA131