N4201Y

Destroyed
Serious

BELLANCA 8KCAB S/N: 294-77

Accident Details

Date
Monday, July 12, 1993
NTSB Number
CHI93LA250
Location
HARVEL, IL
Event ID
20001211X12838
Coordinates
39.350254, -89.530387
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

THE PILOT-IN-COMMAND'S INADEQUATE PREFLIGHT PLANNING.

Aircraft Information

Registration
N4201Y
Make
BELLANCA
Serial Number
294-77
Engine Type
Reciprocating
Model / ICAO
8KCAB BL8
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
ZIELINSKI LYNNE F
Address
6738 RFD
Status
Deregistered
City
LONG GROVE
State / Zip Code
IL 60047
Country
United States

Analysis

On July 12, 1993, about 0917 central daylight time, a Bellanca Decathlon (BL30); N4201Y, was destroyed and the private pilot was seriously injured when the aircraft experienced an engine problem, and impacted the ground. The pleasure flight, originating from Kenosha Municipal Airport, Kenosha, Wisconsin, was operating under 14 CFR Part 91 in visual meteorological conditions with no flight plan on file.

The flight departed Kenosha, Wisconsin approximately 0715 CDT, for St. Jacob, Illinois, on the first leg of a cross country flight to Houston, Texas. The pilot's first planned fuel stop was to be St. Jacob, Illinois (3K6).

Having filled the tanks on July 3, 1993, and making only a short trip from Delavan, Wisconsin to Kenosha, Wisconsin on that day, the pilot assumed she had 33.5 gallons of fuel left when she departed ENW for 3K6 on July 12, 1993.

The pilot reported that "In the general vicinity of the Taylorville Airport, I noticed that the aircraft fuel gauges indicated that the fuel supply was lower than it should have been." She also noticed that the weather was deteriorating, and decided to locate an alternate airport, Taylorville Airport, to check her fuel supply, and also to get an updated weather briefing.

The pilot contacted Taylorville on the Unicom frequency and described some landmarks to them to get a good heading toward the airport. Unable to discern her location, Taylorville suggested a 270 heading and a frequency. After contacting the facility, she was told to squawk a code. At this point, the engine began to sputter. The pilot stated that "It seemed as though I was running out of fuel, but this did not seem possible since I had only flown a little over two hours, and departed with enough fuel for over three hours of flight time."

Realizing she would have to make a forced landing, the pilot lined up with a bean field, and set up for a landing in the field. The aircraft was destroyed during the forced landing.

Investigation found the main fuel filter was approximately half full. The carburetor fuel filter was wet with no significant amount of fuel in the filter cavity. Inspection of the right wing fuel tank revealed a small amount of fuel in the lower rear inboard corner of the tank. The left wing came to rest, inverted, about hte right wing. While rolling the aircraft to expose the top of the left wing, approximately one half pint of fuel ran out of the fuel line from the left tank, which had been cut to facilitate the removal of the pilot. Probing the tank revealed less that a gallon of fuel remaining in the tank.

Medical personnel stated that they noticed a definite lack of fuel smell or visible fuel during the removal of the pilot.

Post-accident examination revealed no evidence of pre-impact mechanical malfunction with airframe, engine or accessories.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI93LA250