N9772L

Substantial
None

BEECH 23 S/N: MC1389

Accident Details

Date
Sunday, August 22, 1993
NTSB Number
CHI93LA331
Location
MILWAUKEE, WI
Event ID
20001211X13111
Coordinates
42.979667, -87.899574
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the student pilot's improper recovery from a bounced landing.

Aircraft Information

Registration
N9772L
Make
BEECH
Serial Number
MC1389
Engine Type
Reciprocating
Model / ICAO
23 BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
STANE DONALD J
Address
120 WOODSIDE LN PO BOX 186
Status
Deregistered
City
ELM GROVE
State / Zip Code
WI 53122
Country
United States

Analysis

On August 22, 1993, at 1030 hours central daylight time, a Beech BE23, N9772L, piloted by the student pilot/airplane co-owner, sustained substantial damage during a bounced landing at Milwaukee Timmerman Airport, in Milwaukee, Wisconsin. The solo student pilot reported no injuries. Visual meteorological conditions prevailed for the flight, a VFR flight plan was filed. The flight operated under 14 CFR Part 91, and originated from Milwaukee, Wisconsin about 0930 hours.

The student pilot departed Milwaukee on a VFR flight plan, with an intended destination of Green Bay, Wisconsin. About 30 minutes after departure, the student pilot made a weather related decision to cancel the cross country and return to Milwaukee. She entered the traffic pattern for Runway 22R. According to witnesses, the first approach to Runway 22R was too high and ended in a go-around. The student pilot stated the second approach to landing "...seemed correct...VASI lights aided my glide and (I) kept on centerline. I crossed threshold with flaps extended, during landing roll...throttle was closed and I raised the flaps to help braking effectiveness. The nose of the aircraft came up, I held controls back slightly. The nose gear went down and up again... ." Witnesses observed the airplane bounce twice before the nosewheel failed. The airplane skidded to a stop on the runway.

The student pilot reported 104 hours total flight time, all accrued in the accident make and model aircraft. She had logged 12 hours in the preceding 90 days, and satisfactorily completed a stage check on June 10, 1993.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI93LA331