N24685

Substantial
None

BEECH 19 S/N: MB-574

Accident Details

Date
Tuesday, August 31, 1993
NTSB Number
NYC93LA181
Location
WOLFBORO, NH
Event ID
20001211X13253
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's failure to abort the takeoff which resulted in an overrun of the runway. Factors were a dirt bank, and the pilot's premature lift off, his failure to attain adequate airspeed, and his lack of recency of experience.

Aircraft Information

Registration
N24685
Make
BEECH
Serial Number
MB-574
Engine Type
Reciprocating
Model / ICAO
19 BE19
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
K R ROBINSON COMPANY
Address
PO BOX 1216
Status
Deregistered
City
ORANGE
State / Zip Code
CT 06477
Country
United States

Analysis

On Tuesday, August 31, 1993, at 1330 eastern daylight time, a Beech BE-19, N24685, registered to K. R. Robinson, Inc., and piloted by Kendall A. Knox, sustained substantial damage during an attempted takeoff from the Lakes Regional Airport, Wolfboro, New Hampshire. The pilot and passenger were not injured. Visual meteorological conditions prevailed, and no flight plan was filed. The flight was being conducted under 14 CFR 91.

The pilot initiated a takeoff on runway 30. In his report, the pilot stated:

The aircraft accelerated to 45 mph and the nose- wheel came off the runway. The A/C continued to accelerate to 60 mph and the main gear came off the runway. The elevator was relaxed slightly in an attempt to accelerate in ground effect and avoid an imminent stall...however the aircraft settled back down onto the runway. The airspeed was between 55-60 mph and the A/C came off the runway again, but only briefly and again settled down failing to climb. At this point the A/C left the paved runway...through...piles of dirt...

Mr. Thomas C. Schultz, Aviation Safety Inspector for the Federal Aviation Administration (Airworthiness), conducted an examination of the wreckage and an interview with the pilot. In his report, Mr. Schultz stated:

The pilot stated that the run-up and power check were normal. When he attempted to take off...he lifted the nose at 45 MPH The aircraft lifted then settled back to the runway. He lowered the nose and accelerated to about 60 MPH, and lifted the nose again and the aircraft lifted then settled back again. ...the aircraft departed the end of the runway, hit some piles of dirt.

His report continued:

When asked if the nose high attitude was higher than usual he said YES. When asked if the aircraft just mushed forward down and off the end of the runway, he again said YES...

Mr. Schultz's report also stated:

On [October 1, 1993] an engine run was accomplished on the above engine while still attached to the fuselage....The engine was started with no difficulty.. ..No malfunction was found that could have caused the accident.

The pilot reported that his total flight time within the 90 days prior to the accident was 1.5 hours.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC93LA181