N757NA

Unknown
None

BOEING 757-200ER S/N: 24567

Accident Details

Date
Monday, September 13, 1993
NTSB Number
BFO93IA175
Location
JAMAICA, NY
Event ID
20001211X13324
Coordinates
40.650669, -73.790794
Aircraft Damage
Unknown
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
85
Total Aboard
85

Probable Cause and Findings

THE FAILURE OF THE LEFT HYDRAULIC PRESSURE SWITCH, WHICH CAUSED THE LEFT YAW DAMPER MODULE TO BECOME INOPERATIVE RESULTING IN UNCOMMANDED RUDDER MOVEMENTS DURING FLIGHT.

Aircraft Information

Registration
N757NA
Make
BOEING
Serial Number
24567
Engine Type
Turbo-jet
Year Built
1990
Model / ICAO
757-200ER B752
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
AWMS I
Address
C/O ANSETT WORLDWIDE AVIATION SVC
445 PARK AVE 20TH FLOOR
Status
Deregistered
City
NEW YORK
State / Zip Code
NY 10022-2606
Country
United States

Analysis

On September 13, 1993, about 0855 hours eastern daylight time, N757NA, a Boeing 757-200ER, operating as North American Airlines Flight 5, had a flight control problem during cruise flight. The flight had departed from John F. Kennedy International Airport (JFK), Jamaica, New York, en route to San Francisco, California, but returned to JFK and landed uneventfully. None of the eight crewmembers or 77 passengers were injured. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed. The flight was conducted under 14 CFR 121.

According to a FAA aviation safety inspector, a "rudder ratio" warning message was displayed in the cockpit as the airplane climbed through Flight Level 270 after departure. The crew performed the published company troubleshooting procedures, including resetting the rudder ratio circuit breaker light, and the warning was eliminated. About one hour later during cruise flight at Flight Level 350, the warning was displayed once again followed by gradual uncommanded right rudder movement. The autopliot was engaged at the time and two units of left aileron were inputted by the autopilot. The airplane remained under control and the crew counteracted the rudder movement manually. The captain elected to abort the flight and return to JFK.

An examination of the airplane's electrical system revealed that the fault ball on right rudder control module had popped out. The module was reset and successfully passed a functional check. The airplane was placed back into service.

The rudder ratio warning message was again displayed on two flights subsequent to this event. The flights terminated uneventfully. According to company maintenance records, maintenance activities to correct the situation during these events involved readjustment of the rigging, functional testing of the fault module, and replacement of the rudder ratio actuator. The airplane was placed back into service after each of these events.

On November 19, 1993, the rudder ratio light was displayed for the fourth time in about two months. An examination of the left yaw damper module revealed a malfunction in the left hydraulic pressure switch. The unit was removed and replaced. No further incidents involving a rudder ratio problem were reported.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO93IA175