N193CW

Substantial
Minor

WILSON KIT FOX MODEL 4 S/N: 1572

Accident Details

Date
Wednesday, September 8, 1993
NTSB Number
BFO93LA166
Location
BOWDOINHAM, ME
Event ID
20001211X13342
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

LOSS OF ENGINE POWER FOR AN UNDETERMINED REASON.

Aircraft Information

Registration
N193CW
Make
WILSON
Serial Number
1572
Model / ICAO
KIT FOX MODEL 4

Registered Owner (Historical)

Name
OLSON CLIFFORD JAY
Address
3605 OAKVILLE WALTZ RD
Status
Deregistered
City
NEW BOSTON
State / Zip Code
MI 48164-9669
Country
United States

Analysis

On Wednesday, September 8, 1993, at about 1400 eastern daylight time, a Kit Fox Model 4, N193CW, owned and operated by Charles Cunningham of Bowdoinham, Maine, and Robert Wilson of Brunswick, Maine, and piloted by Charles Cunningham, lost total engine power shortly after takeoff from runway 14 at the Merrymeeting airport located in Bowdoinham. The airplane collided with trees during the subsequent forced landing and was substantially damaged. The pilot received minor injuries. Visual meteorological conditions prevailed at the time of the accident. The local flight was conducted under 14 CFR Part 91.

The pilot stated that shortly after takeoff, the airplane's Rotax two cylinder engine lost total power. He stated he tried to reverse direction and land the airplane on runway 32. He stated the airplane did not have enough altitude to clear the trees at the approach end of the runway. The airplane impacted the trees and came to rest on the treetops about 50 feet above the ground.

Post accident examination of the engine was accomplished and no anomalies were noted. Fuel was found in the fuel tanks and fuel lines leading to the engine. The engine was started and ran without any anomalies noted. The engine failure could not be duplicated.

The pilot stated that the airplane's engine had lost total power on a previous flight. He stated that he thought the problem was with the airplane's electronics because the tachometer was "very erratic." He stated he checked all the airplane's electronic equipment and could not duplicate the problem. The pilot stated that he thought the engine's double coil was "shorting out."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO93LA166