N80010

Destroyed
None

BEECH A36 S/N: E-2749

Accident Details

Date
Monday, September 27, 1993
NTSB Number
FTW93LA266
Location
HOUSTON, TX
Event ID
20001211X13409
Coordinates
29.650094, -95.280685
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

THE FUEL LEAK WHICH RESULTED FROM THE MECHANIC'S IMPROPER INSTALLATION OF THE FUEL LINE. A FACTOR WAS THE LEAD MECHANIC'S INADEQUATE POST RUN UP INSPECTION.

Aircraft Information

Registration
N80010
Make
BEECH
Serial Number
E-2749
Engine Type
Reciprocating
Model / ICAO
A36 BE36
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
UNITED BEECHCRAFT INC
Address
PO BOX 2966
Status
Deregistered
City
WICHITA
State / Zip Code
KS 67201
Country
United States

Analysis

On September 27, 1993, at approximately 1510 central daylight time, a Beech A36, N80010, was destroyed by fire during engine start at the Hobby Airport, in Houston, Texas. The airplane, being flown by an ATP rated pilot, was about to depart on a local flight. There was no flight plan filed and visual meteorological conditions prevailed throughout the area. Neither the pilot nor the passenger were injured.

According to the pilot, who was a Beech sales person, the flight was to be an acceptance flight prior to sale to the passenger. The pilot stated that he utilized the high boost pump to pressurize the system and then started the engine. The engine started and then quit. He applied boost pump again and restarted. During the second start, the pilot noted flames coming up from the engine compartment toward the cockpit door window. The pilot and the passenger immediately exited the airplane prior to its being engulfed in flames. The pilot failed to return the Pilot/Operator Accident Report that was provided to him following the accident.

Investigation revealed a cross threaded output line on the engine driven fuel pump which allowed fuel to leak into the engine compartment. The fuel pump had been removed earlier in the day for compliance with a service bulletin and re-installed. Following the completion of the maintenance, the airplane was run up by the lead mechanic who stated that he also performed a post- run inspection. He later stated to his supervisor that during the run up he had to keep the electric boost pump operating in the low position to prevent the engine from running rough. However, he did not relate the situation until after the mishap.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW93LA266