N5151A

Substantial
None

CESSNA O-2A S/N: 68-6873

Accident Details

Date
Friday, October 1, 1993
NTSB Number
LAX94LA001
Location
TUCSON, AZ
Event ID
20001211X13584
Coordinates
32.059345, -111.419342
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

was the partial loss of engine power during initial climb due to partial clogging of the engine's fuel injectors. Blockage of the fuel injectors was due to inadequate maintenance of the fuel system by contract maintenance personnel.

Aircraft Information

Registration
Make
CESSNA
Serial Number
68-6873
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
O-2A CN1
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
6
FAA Model
O-2A

Registered Owner (Current)

Name
SIMMERMAN STEVEN C
Address
1707 KIRBY PKWY
City
MEMPHIS
State / Zip Code
TN 38120-4367
Country
United States

Analysis

On October 1, 1993, at 1220 mountain standard time, a Cessna O- 2A, N5151A, experienced a partial loss of engine power to the front and rear engines during initial climb from the Ryan Field near Tucson, Arizona. The pilot made a forced landing in an open field about two miles east of the airport. The airplane was substantially damaged upon impacting the rough, desert terrain. The commercial pilot was not injured. The flight was originating at the time of the mishap.

The pilot verbally reported that prior to the accident flight the airplane had been idle for several years. The pilot had been hired to ferry the airplane from Arizona to the southeast United States. In preparation for the flight, a contractor had performed limited maintenance on the airplane.

According to the pilot, during takeoff the airplane's front engine suddenly lost power. Its rpm reduced from full power to about 1,600 rpm, and then the rear engine lost power. The fuel flow became "low and intermittent" and the airplane stopped climbing. The pilot further reported that because the engines' oil temperature and pressure remained in the normal operating range, he believed both engines had experienced fuel starvation.

On October 7, 1993, a Federal Aviation Administration (FAA) airworthiness inspector verbally reported to the National Transportation Safety Board that its examination of the airplane revealed two of the front engine's six fuel injectors were found partially clogged with a foreign substance. The FAA inspector stated that the contractor had evidently not completely purged the airplane's entire fuel system during efforts at preparing the airplane for the ferry flight.

In October of 1993 and in May of 1994, the pilot was requested to complete the required Safety Board "Aircraft Accident Report," NTSB Form 6120.1. When the Board receives the pilot's form, it will be appended to this report.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX94LA001