N2656R

Substantial
None

Cessna 182K S/N: 18258356

Accident Details

Date
Saturday, May 22, 1999
NTSB Number
SEA99LA078
Location
KALISPELL, MT
Event ID
20001212X18902
Coordinates
48.190895, -114.380935
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power for undetermined reasons. Rough terrain was a factor.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18258356
Engine Type
Reciprocating
Model / ICAO
182K C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
182K

Registered Owner (Current)

Name
EDEX AVIATION LLC
Address
12861 SHAKE RIDGE RD
City
SUTTER CREEK
State / Zip Code
CA 95685-8200
Country
United States

Analysis

On May 22, 1999, approximately 1445 mountain daylight time, the pilot of a Cessna 182K, N2656R, attempted a forced landing in a rough field after experiencing a complete loss of engine power while taking off from Kalispell City Airport, Kalispell, Montana. The commercial pilot, who was the sole occupant, was not injured, but the aircraft, which was owned and operated by Angle View Air, sustained substantial damage. The 14 CFR Part 91 glider towing flight was being operated in visual meteorological conditions, and no flight plan had been filed.

According to the pilot, he had towed the glider to about 350 feet above the ground (AGL) when the engine started slowing and then stopped. He immediately released the glider, which successfully returned to the airport, and then attempted a forced landing in an open field. Although the touchdown was successful, the aircraft sustained damage while rolling across the rough uneven field.

Shortly after the accident, a local mechanic inspected the airplane for damage. The mechanic reported that the firewall was damaged, the fuselage belly displayed wrinkles to the skin, and the nose wheel was bent about 10 degrees off center. The mechanic then started the engine and did a run-up, to include checking the carburetor heat control. The test run was completed with no mechanical failures or malfunctions noted. The next day, an individual flew the airplane out of the field and returned it to the Kalispell City Airport.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA99LA078