N41078

Destroyed
Fatal

Piper PA-31-350 S/N: 31-8352017

Accident Details

Date
Friday, June 11, 1999
NTSB Number
ANC99FA074
Location
TANANA, AK
Event ID
20001212X18907
Coordinates
65.179054, -152.069946
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Undetermined.

Aircraft Information

Registration
N41078
Make
PIPER
Serial Number
31-8352017
Engine Type
Reciprocating
Model / ICAO
PA-31-350 PA31
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
CHARTERCRAFT LEASING & SALES INC
Address
7650 W COURTNEY CAMPBELL CSWY
STE 1120
Status
Deregistered
City
TAMPA
State / Zip Code
FL 33607-5955
Country
United States

Analysis

HISTORY OF FLIGHT

On June 11, 1999, about 0723 Alaska daylight time, a Piper PA-31-350 airplane, N41078, was destroyed by impact with trees and the Yukon River, about 1.5 miles southwest of Tanana, Alaska. The airplane was being operated as Flight 1604 from Fairbanks, Alaska, to Tanana, to Galena, Alaska, as a visual flight rules (VFR) scheduled passenger/cargo flight under Title 14, CFR Part 135. The airplane was operated by Larry's Flying Service Inc., Fairbanks. The certificated airline transport pilot, the sole occupant, received fatal injuries. Visual meteorological conditions prevailed. VFR company flight following procedures were in effect.

Flight 1604 departed Fairbanks about 0631 and was carrying cargo only. The flight landed at the Ralph M. Calhoun Memorial Airport, Tanana about 0712. According to the operator's records, 109 pounds of cargo was unloaded. About 1,236 pounds of cargo remained on the airplane. The airplane departed runway 24 about 0718 for Galena.

A witness at the airport saw the airplane arrive in Tanana. He said the engines sounded normal. When the engines were started for departure, he noted the right engine was started first after extended cranking. Once started, the right engine ran at a high idle. The left engine was then immediately started. It ran at a lower rpm, and sounded normal. The witness saw the airplane depart, and said that after the landing gear retracted, the airplane leveled off and stayed low over the river. The airplane turned to follow the Yukon River instead of climbing.

A village agent for the operator reported he heard the airplane arrive in Tanana, and it sounded normal. He departed the airport before the airplane took off. About five minutes after he left the airport, he heard a loud noise from the river area. He heard a loud bang, followed by a loud screeching noise, and then quiet.

About five minutes after departure, the pilot contacted a local weather observation service at Tanana on the common traffic advisory frequency (CTAF). The pilot radioed that he was having a problem with the airplane, and stated he may have to ditch. He did not describe the nature of the problem. About 15 seconds later, the pilot radioed that he was over the river, the airplane was clipping trees, and he was attempting to return to the runway.

The airplane collided with several trees located on a small island in the Yukon River, separating the outboard end of the left wing. The airplane then collided with the water and sank.

The accident occurred during the hours of daylight at latitude 65 degrees, 09.5 minutes north, and longitude 152 degrees, 09.4 minutes west.

CREW INFORMATION

The pilot held an airline transport pilot certificate with an airplane multiengine land rating. He held commercial pilot privileges with airplane single-engine land and sea ratings. The most recent first-class medical certificate was issued to the pilot on February 25, 1999, and contained no limitations.

The pilot was an enlisted member of the U.S. Air Force. His previous 72 hour military schedule was provided by personnel from the Eielson Air Force Base, Fairbanks. The pilot was on duty with the Air Force from 1800, June 7, to 0600, June 8. He was scheduled to be off duty from June 9, to June 11.

According to flight and duty records provided by the operator, the pilot logged 2.4 hours of flight time for the operator on June 9, from 0830 to 1100. On June 10, he logged 4.3 hours from 0630 to 1330. His anticipated flight time on June 11, was to be a repeat of the previous day. The pilot's personal flight logs were not located.

The pilot was hired by the operator on March 7, 1996. According to the operator, the pilot had accrued 3,226.7 hours of total experience, 861.2 of which were in the accident airplane make and model. In the previous 12 months before the accident, the pilot accrued 826.7 hours, of which 611.2 were in the accident airplane make and model. In the previous 30 days, the pilot accrued 51.2 hours, and 48.7 in the accident airplane. In the previous 24 hours, the pilot accrued 5.3 hours in the accident airplane.

AIRCRAFT INFORMATION

The airplane was maintained on a phase inspection program, as part of a Federal Aviation Administration (FAA) approved aviation inspection program (AAIP). A complete inspection of the airplane consists of four event inspections, each accomplished every 55 hours, for a total of 220 hours for the entire cycle. A complete inspection cycle is required to be accomplished within a 12 calendar month period, and qualifies as an annual inspection for the airplane. Each event inspection consists of detail items, and routine items. According to the AAIP, A routine inspection consists of a visual examination or check of items, as practical, without disassembly. A detailed inspection consists of an examination necessitating disassembly of items, as required. Each event inspection includes maintenance discrepancy items that are in addition to those specifically listed in the AAIP.

The most recent inspection of the airplane was an Event Four inspection, conducted on June 4, 1999. The inspection consisted of a detailed inspection of the right engine, the right propeller, the right engine turbocharger, and the landing gear. A routine inspection of the left engine, the left propeller, the left engine turbocharger, and fuselage, was also part of the Event Four inspection.

At the last inspection, the airplane had accrued 15,208.9 hours total time. The left and right engines had 1290.3 hours since overhaul. Both engines were overhauled by the operator on February 14, 1998. The left propeller had accrued 2128.6 hours since overhaul. The right propeller had accrued 1871.8 hours since overhaul.

Since the last inspection, until the airplane departed for Tanana on the day of the accident, the airplane accrued an additional 20.5 hours. Examination of the maintenance records revealed no uncorrected discrepancies since the last inspection.

Examination of the maintenance records disclosed several fuel system related discrepancies from January 1999, to June, 1999. During an Event Four inspection on January 4, 1999, the right engine fuel pump had evidence of a slight leak. It was retorqued. The right wing fuel sump drain was leaking. The sump valve was replaced. During an Event One inspection on January 22, 1999, the airplane fuel regulator was leaking. It was replaced. During an Event Two inspection on February 22, 1999, fuel stains were noted in the left engine accessory section. The fuel line to the fuel pump was tightened. During an Event Three inspection on March 18, 1999, the right engine's number one cylinder induction tube had signs of a fuel leak. New gaskets were installed. During an Event Four inspection on April 6, 1999, the right engine fuel pump had signs of fuel leaking around the adjustment head. The pump was retorqued. The left engine fuel pump had signs of fuel staining. A fitting on the pump was cleaned and resealed. During an Event Two inspection on May 6, 1999, a fuel leak was noted on the number 2 cylinder on the left engine. A bolt was replaced on the intake pipe flange. The fuel line to the airplane heater had signs of fuel staining. The fuel line fitting was tightened. During an Event Three inspection on May 23, 1999, the number three and number five cylinder induction tubes on the right engine were leaking. The gaskets were replaced.

The maintenance records note that during the Event Four inspection on April 6, 1999, a discrepancy was noted that stated, "left engine - wrench sticking out of engine by alternator." The sign-off for the discrepancy was, "removed wrench and returned to proper location."

The pilot's operating handbook for the accident airplane specifies the use of zero flaps for a normal takeoff, and 15 degrees of flaps for a short field takeoff. After takeoff, the flaps are retracted before the airplane reaches 128 knots.

The pilot's handbook specifies airplane's minimum controllable airspeed is 76 knots. The best single-engine angle of climb speed is 104 knots. The best single-engine rate of climb speed is 106 knots.

The emergency engine inoperative procedure for engine securing (feathering procedure), specified in the pilot's handbook states, in part: Throttle, close; Propeller, FEATHER; Mixture, Idle Cut-Off; Cowl flaps, close...Fuel Selector, OFF (detent).

METEOROLOGICAL INFORMATION

The closest official weather observation station is Tanana, Alaska, which is located 1.5 nautical miles northeast of the accident site. On June 11, at 0652, an Automated Weather Observation Station (AWOS) was reporting in part: Wind, calm; visibility, 40 statute miles; clouds, few at 10,000 feet, few at 18,000 feet; temperature, 57 degrees F; dew point, 48 degrees F; altimeter, 29.90 inHg.

COMMUNICATIONS

The CTAF for the Tanana airport is 122.9 MHz. There is no recording capability of communications at the airport, or with the local weather observer.

AERODROME AND GROUND FACILITIES

The Tanana airport is located along the north shore of the Yukon River. It is equipped with a single gravel surface runway on a 060 to 240 degree magnetic orientation. Runway 24 is 4,400 feet long by 150 feet wide, and is equipped with medium intensity runway lights. Local airport weather observations, (call sign: Tanana Weather), are available on the CTAF.

WRECKAGE AND IMPACT INFORMATION

FAA inspectors from the Fairbanks, Alaska, Flight Standards District Office (FSDO) responded to the area of the accident on June 11. They located an area of impact with several large trees, about 45 feet above the ground, and about 200 feet south of the northwest shoreline of Long Island. From the first observed point of impact in the tree line, heading towards the Tanana Airport, the terrain consisted of, in sequence, a heavily wooded island, a small area of open water, a large gravel bar, another area ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC99FA074