N4198D

Substantial
None

Helio H-395 S/N: 592

Accident Details

Date
Tuesday, July 20, 1999
NTSB Number
ANC99LA095
Location
IGIUGIG, AK
Event ID
20001212X19138
Coordinates
58.749374, -156.539962
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inadequate compensation for wind conditions during the downwind to upwind taxi turn. Factors associated with this accident were the high crosswind, the pilot's improper use of flaps, and his self-induced pressure because he was behind schedule.

Aircraft Information

Registration
N4198D
Make
HELIO
Serial Number
592
Year Built
1963
Model / ICAO
H-395

Registered Owner (Historical)

Name
COPPER RIVER AIRMOTIVE LLC
Address
HC 60 BOX 251B
Status
Deregistered
City
COPPER CENTER
State / Zip Code
AK 99573-9704
Country
United States

Analysis

On July 20, 1999, about 1505 Alaska daylight time, a float equipped Helio H-395 airplane, N4198D, sustained substantial damage during takeoff from Kukaklek Lake, about 18 miles southeast of Igiugig, Alaska, at 59 degrees 07 minutes north latitude, 155 degrees 32 minutes west longitude. The solo commercial pilot was not injured. The airplane was operated under 14 CFR Part 91 by Branham Adventures Limited Partnership of Anchorage, Alaska, in support of a fishing lodge. The flight was departing on a return leg to the Kulik Lake Lodge, Alaska, after dropping off three passengers. Visual meteorological conditions prevailed at the time of the accident, and a company VFR flight plan was filed.

During a telephone interview with the NTSB investigator-in-charge (IIC) on July 21, the company owner stated that the pilot attempted a takeoff with a left crosswind of about 20 knots. The pilot aborted the first takeoff, then performed a downwind water taxi prior to attempting a second takeoff. The owner stated that the pilot left the flaps extended halfway, and commenced a second takeoff. The wind lifted the left wing, and the left float came off the water. The owner indicated the pilot applied power to continue the takeoff, the right float dug into the water, and the airplane nosed over, sustaining substantial damage.

During a personal interview with the IIC on July 22, the pilot said that the wind was about 25 knots near the shore, and stronger toward the center of the lake. He attempted a takeoff with a left crosswind, close to the edge of the lake where there was shelter from the southwest wind. He aborted the first takeoff when he could not get the nose of the airplane to turn to the right, toward the river opening out of the lake. He then water taxied downwind farther into the lake, intending to takeoff into the wind with a longer takeoff run. During the taxi, the pilot did not retract the flaps from the 1/2 position. As he began to turn left, into the wind, the wind lifted the left wing. The pilot said that he had full aileron deflected into the wind, and added power in an attempt to bring the airplane's nose into the wind. He stated the right float dug in, and the airplane nosed over. The pilot also added that he was late for his next pickup, in a hurry, and should not have water taxied in high winds with the flaps extended.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC99LA095