N9785T

Substantial
None

Cessna 172 S/N: 47585

Accident Details

Date
Monday, September 6, 1999
NTSB Number
ATL99LA123
Location
HOUSTON, MS
Event ID
20001212X19690
Coordinates
33.889263, -88.999702
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's failure to switch the magneto switch to the both position before attempting a takeoff that resulted in the loss of engine power and resulted in the subsequent collision with trees.

Aircraft Information

Registration
N9785T
Make
CESSNA
Serial Number
47585
Engine Type
Reciprocating
Year Built
1960
Model / ICAO
172 C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GANN MELVIN E SR
Address
231 COUNTY ROAD 106
Status
Deregistered
City
HOUSTON
State / Zip Code
MS 38851-8743
Country
United States

Analysis

On September 6, 1999, at 1100 central daylight time, a Cessna 172, N9785T, collided with underbrush/trees and nosed over on the departure end of runway 18 at a private airstrip in Houston, Mississippi. The personal flight was operated by the pilot under the provisions of Title 14 CFR Part 91 with no flight plan filed. Visual weather conditions prevailed at the time of the accident. The airplane sustained substantial damage and the commercial pilot received and his passenger were not injured. The flight departed Houston, Mississippi, at 1055.

The pilot reported that he conducted a preflight inspection of the airplane before it was removed from his hangar. Following the preflight inspection, the pilot taxied to runway 18 where he completed a normal engine run-up. During the attempted takeoff, the pilot recalled that the engine did not operate at the normal takeoff performance level. After liftoff from the 1600-foot sod airstrip, the pilot recalled that the airplane would not climb. The airplane collided with 30 foot tall trees and underbrush, and nosed over about 50 feet from the departure end of the runway.

During a telephone conversation, the pilot stated that he completed the engine run-up procedure as he taxied to the runway for takeoff. He reported that all systems checked normal, but he believed he forgot to return the magneto switch to the both position before attempting the takeoff. He also said, he and his son had previously completed several takeoffs from their private airstrip and they were usually airborne within the first half of the 1600-sod airstrip.

No mechanical problems were reported by the pilot. The post-accident examination of the airplane also failed to disclose a mechanical problem.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL99LA123