N4527K

Substantial
None

Navion A S/N: NAV-4-1527

Accident Details

Date
Thursday, September 9, 1999
NTSB Number
CHI99LA340
Location
UTICA, NE
Event ID
20001212X19714
Coordinates
40.889068, -97.339210
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the failure of the fuel pump and the misjudged touchdown point by the pilot. A factor was the high vegetation.

Aircraft Information

Registration
N4527K
Make
NAVION
Serial Number
NAV-4-1527
Engine Type
Reciprocating
Year Built
1948
Model / ICAO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WHITESEL MANAGEMENT COMPANY INC
Address
7200 270TH RD
Status
Deregistered
City
MILLER
State / Zip Code
NE 68858-2052
Country
United States

Analysis

On September 9, 1999, at 1736 central daylight time, a Navion model A, N4527K, piloted by a private pilot, sustained substantial damage during a forced landing, to runway 35 (3,000 feet by 50 feet, dry/concrete), at the Flying V Airport, Utica, Nebraska, following an engine failure during cruise flight. The aircraft impacted terrain short of the approach end of the runway. The personal flight was conducted under the provisions of 14 CFR Part 91 and was not on a flight plan. Visual meteorological conditions prevailed at the time of the accident. The pilot reported no injuries to himself or his one passenger. The flight originated from the Lincoln Municipal Airport, Lincoln, Nebraska, at 1710 and was en route to the Kearney Airport, Kearney, Nebraska.

In a written statement, the pilot said, "... at 4,500 feet, the engine died suddenly and completely. I immediately turned on [the] boost pump, which did no good. I then, turned back 180 degrees and headed for NE23 (Utica, NE) which we had just passed. I notified Lincoln App [approach] of our problem and that re-start procedures didn't work." The pilot then said, "I thought I was set up to touch down halfway down the runway, let [the] gear down, got three lights, and then pumped down the rest of the flaps." The pilot said that he touched down approximately 150 feet from the end of the runway and on rollout the landing gear collapsed due to the presence of "...five feet tall fireweeds."

During a post accident examination of the airplane, the engine driven fuel pump drive pin was found to be sheared. No other preexisting anomalies were found with respect to the aircraft or its systems.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI99LA340