N6676V

Substantial
None

Bellanca BL-17-30 S/N: 30046

Accident Details

Date
Saturday, September 11, 1999
NTSB Number
MIA99LA251
Location
ATHENS, GA
Event ID
20001212X19829
Coordinates
34.000289, -83.340591
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The pilot's improper fuel management resulting in loss of engine power on approach due to fuel starvation and damage to the aircraft during the subsequent forced landing.

Aircraft Information

Registration
N6676V
Make
BELLANCA
Serial Number
30046
Year Built
1967
Model / ICAO
BL-17-30

Registered Owner (Historical)

Name
LOPEZ CLAUDIO JR
Address
240 PINERIDGE RD
Status
Deregistered
City
BOGART
State / Zip Code
GA 30622-1942
Country
United States

Analysis

On September 11, 1999, about 1325 eastern daylight time, a Bellanca Super Viking BL-17-30, N6676V, registered to Century Restorations and Sales, Inc., operating as a Title 14 CFR Part 91 personal flight, crashed on approach to Athens/Ben Epps Airport, Athens, Georgia. Visual meteorological conditions prevailed and no flight plan was filed. The airplane sustained substantial damage and the airline transport-rated pilot and two passengers were not injured. The flight originated from the same airport about 20 minutes before the accident.

According to the pilot, he and his son and stepson intended to fly, "one or two laps around the pattern." His fuel distribution for the takeoff was full auxiliary tanks, about 10 gallons in the right main, and 5 or 6 gallons in the left main. After takeoff and a left downwind turn from runway 09, he requested an extended downwind leg to overfly downtown and the stadium. Following the overfly that lasted about 20 minutes and while established on approach for runway 09, at about 2 miles out, he experienced engine surging. He switched his fuel selector to an auxiliary tank, and activated his boost pump, and the engine smoothed out for 4 or 5 seconds before it resumed the surging. Engine power available was not enough to sustain flight to the runway, and he attempted a forced landing to a parking lot/driveway about 1/2 mile short of the runway. The pilot later characterized the occurrence stating that he ran out of fuel in the right main tank, switched to an aux tank, and didn't have enough time or altitude for the engine to restart.

According to an FAA inspector, once the airplane impacted the parking lot, it slid for about 340 feet, tearing off the right wing and horizontal stabilizer, and damaging a residential fence. Examination of the fuel distribution aboard revealed the left auxiliary was 1/2 full, right auxiliary was destroyed, left main contained a trace amount and nothing usable, and the right main contained about 2 to 3 inches. The fuel selector was found on the right auxiliary position, and the ground showed evidence of fuel spill from that tank.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA99LA251