N29362

Substantial
None

Cessna 177 S/N: 17700840

Accident Details

Date
Thursday, October 7, 1999
NTSB Number
NYC00LA024
Location
FRANKFORT, KY
Event ID
20001212X20043
Coordinates
38.189250, -84.859176
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

A total loss of engine power for undetermined reasons

Aircraft Information

Registration
Make
CESSNA
Serial Number
17700840
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
177 C177
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
177

Registered Owner (Current)

Name
HUDGINS ERIC D
Address
PO BOX 14635
City
NEWPORT NEWS
State / Zip Code
VA 23608-0013
Country
United States

Analysis

On October 7, 1999, about 1945 Eastern Daylight Time, a Cessna 177, N29362, was substantially damaged during a forced landing at Frankfort, Kentucky. The pilot and two passengers were not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight conducted under 14 CFR Part 91. The flight departed Willow Island Airpark, Finchville, Kentucky; and was destined for Capital City Airport (FFT), Frankfort, Kentucky.

According to the pilot's written statement:

"...About 3 or 4 miles west of the Frankfort Airport the engine quit...I landed [in a field] going up hill and the nose gear folded on the way down the other side. The prop had stopped before we landed and wasn't bent. We got out and walked away."

During a telephone interview, the pilot stated that the airplane had a Supplemental Type Certificate for automobile gasoline. He added 15 gallons of automobile gasoline to the airplane before the flight. The pilot originally purchased the gasoline at an automobile gas station. He believed the fuel filter became clogged due to fuel contamination.

The pilot submitted a National Transportation Safety Board Pilot/Operator Aircraft Accident Report Form. According to the form, the airplane's engine was remanufactured on November 19, 1975. At the time of the accident, it had approximately 2,100 hours of operating time since the date of remanufacture.

Examination of the wreckage by a Federal Aviation Administration Inspector did not reveal any pre-impact mechanical malfunctions. The Inspector observed fuel in both fuel tanks. He did not find any debris in the fuel filter.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC00LA024