N576NL

Substantial
Serious

Hawker Siddeley HUNTER T MK 7 S/N: 41H003314

Accident Details

Date
Wednesday, November 17, 1999
NTSB Number
LAX00LA034
Location
MESA, AZ
Event ID
20001212X20120
Coordinates
33.329875, -111.630607
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
1
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The fatigue failure and separation the stage 3 compressor blades due to corrosion pitting of the blade retention lug bores. A factor in the accident was the failure of the various post military surplus operators of this engine to incorporate the manufacturer's recommended modifications to prevent such failures.

Aircraft Information

Registration
N576NL
Make
HAWKER SIDDELEY
Serial Number
41H003314
Engine Type
Turbo-jet
Model / ICAO
HUNTER T MK 7 HUNT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MACH TWO INC
Address
1013 CENTRE RD STE 301
Status
Deregistered
City
WILMINGTON
State / Zip Code
DE 19805-1265
Country
United States

Analysis

On November 17, 1999, at 1649 hours mountain standard time, a Hawker Siddeley Hunter T MK 7 jet, N576NL, collided with a ditch following a complete power loss on initial takeoff at Williams-Gateway Airport, Mesa, Arizona. The airplane, owned by Mach Two Inc. and operated by Advanced Training Systems International, Inc., sustained substantial damage. The commercial pilot sustained serious injuries and his passenger received minor injuries. The flight was being conducted under 14 CFR Part 91 when the accident occurred. The purpose of the flight was to reposition the aircraft to California for training purposes. Visual meteorological conditions prevailed at the time of the accident and the airplane was on an IFR flight plan. The flight originated at the airport moments before the accident.

The pilot said that the airplane was prepared for flight and serviced by his crew chief before he did a preflight on the airplane. He stated that everything appeared ok and the airplane appeared ready for flight. The pilot said the engine start was uneventful, "nice and cool," with temperatures staying below 500 degrees as the engine spooled up to idle power in less than 20 seconds. He requested and received an IFR clearance to NAS Pt. Mugu from ground control, went through the post start and taxi checks, and taxied out to runway 30C. After they reached the hold short line, they completed the takeoff checklist and called for takeoff. They were cleared for takeoff with a right turnout after departure.

The pilot said they taxied out on the runway and ran the engine up to 7,200 rpm and checked the instruments and flight controls. The engine temperature, oil pressure, hydraulic pressure, and boosted flight controls were working well. He then released the brakes, pushed the throttle up to the "military power detent," and checked the instruments again as they began the takeoff roll. He stated that rpm was 8,100, temperature was 650 degrees, and oil and hydraulic pressure was good. He said the airplane accelerated nicely and he rotated at 130 knots and flew off at 140 knots after using about 3,000 feet of take-off roll.

About 5-10 seconds after takeoff, the pilot said he experienced a significant compressor stall with the engine "chug" and a loud explosion. He notified the crew chief that they had just lost the engine, and that he was going to set the airplane back down. He lowered the landing gear and set up for a normal touchdown back on the runway. He extended the drag chute just before touchdown and said he felt a "good tug." Once back on the ground, he immediately began applying the brakes in an attempt to stop the airplane before they reached the flood control ditch at the end of the runway. He was unable to stop the airplane before it hit the ditch and they went into the ditch and back out the other side. When the airplane came to rest, the pilot said he told his crew chief that he had broken his back and asked him to blow the canopy for him to get them out of the airplane.

The crew chief, positioned in the right seat, stated that the preflight, start-up, run-up, and takeoff were "normal," and he did not realize that there was a problem until the pilot informed him that the engine had quit. He said he did not recall seeing any panel lights or hearing any aural warnings.

An eyewitness to the crash said he was located on the south ramp at the airport and that the ramp was approximately 45-degrees to the runway. His line-of-sight had him watching the middle of the takeoff run. He said he heard a "bang" which sounded like a compressor stall and then the airplane was out of his sight. He said he heard two more compressor stalls at close to the same magnitude. He said he would estimate the airplane was at 100 feet agl when he first noticed the takeoff.

A witness, who was a pilot in an airplane behind the accident airplane, was interviewed. He stated he observed a 30-foot flame exit the engine when it was about 200 feet above the ground on the initial takeoff climb. The pilot said that he did not observe any catastrophic failure of the engine or any parts depart the engine as he observed the flames.

One eyewitness who watched the airplane takeoff stated he heard a "bang" that sounded like a compressor stall after the airplane had climbed to approximately 100 feet agl. He said the airplane continued out of his sight but that he heard at least two other loud noises very similar to the first noise after the airplane disappeared from his sight.

AIRCRAFT INFORMATION

The airplane is a two-seat ex-military jet fighter produced in the 1950's and early 1960's by Hawker for service in the United Kingdom Royal Air Force. Following the airplane's surplus from the RAF, it was imported into the United States and was being flown under a Federal Aviation Administration (FAA) special airworthiness certificate in the experimental category for the purpose of exhibition and racing. The airworthiness certificate was issued on December 12, 1994, by the Minneapolis, Minnesota, Flight Standards District Office.

The airplane's logbook shows three recent flights including the ferry flight from Minnesota to Williams Gateway on November 9, 1999, for a total of 3.5 hours. The pilot of the ferry flights was also the pilot on the accident flight.

According to Rolls-Royce, a review of their records indicated that the engine, serial number 5919, was manufactured in 1954 and sent to the RAF as part of a spares contract. The engine was last dispatched from their overhaul facility on March 26, 1981, following part life rework (overhaul) at 251 hours technical service order (TSO). According to Rolls-Royce, the engine is life limited (overhaul requirement) at 450 hours from parts rework and it would be life expired at 701 hours TSO. The last records on this engine documented its installation in another Hawker Hunter, serial number XL617, by the RAF on September 28, 1983, with 392 hours TSO.

The engine maintenance records presented by the operator at the request of Safety Board investigators began on June 27, 1990, and documented its installation in the accident airframe at Volk Field, Wisconsin. An unsigned handwritten note preceded this entry and stated that the engine had a total run time since overhaul of 436 hours, with 265 hours remaining to life limit. No documentation was available to support the engine history between leaving RAF service and the installation in the accident airframe. The last entry in the records was dated July 2, 1999, and consisted of an annual inspection at a time of 548 hours since overhaul.

WRECKAGE INSPECTION

Safety Board investigators and technical representatives of Rolls-Royce examined the airplane on January 11-12, 2000. The salvage operator who recovered the airplane reported that the main fuselage fuel tanks and 100-gallon tip tanks were full of fuel, with just in excess of 400 gallons pumped into barrels at the crash site. The wings were removed by the salvage operator to assist in the recovery of the airplane. The nose gear was collapsed and the nose bay was damaged. Impact damage was observed to the forward section of the fuselage. Inspection of the intake prior to the engine removal showed that the intake ducting contained a moderate amount of dirt, with heavier concentrations present in the right duct. The starter fairing was intact with no apparent damage. The left portion of the instrument panel just above the avionics rack was buckled. All circuit breakers were in. The LP and HP throttle cocks were in the aft (cutoff) position. The fuel isolation switch was guarded and in the normal position.

The engine remained contained within the engine bay during the impact sequence. Further examination of the engine revealed that the forward roller track was fractured. The bottom of the exhaust duct showed upward bending. The aft portion of the tail cone contained evidence of fire damage external to the tail cone. Material burn through was evident extending from an area at the 6 o'clock position to the 3 o'clock position as viewed from the rear. The tail cone also had impact deformation. Inspection of the exhaust duct area revealed a heavy deposit of black foreign material between blades of the LP turbine. The deposit was noted to be centrifuged to the shroud ID and was brittle in nature. Additionally, the exterior contained a black brittle appearance. The deposits broke into pieces when removed with a small screwdriver.

Control continuity was established to the LP and HP throttle levers at the FCU prior to engine removal.

The engine accessories were found undamaged after the engine was removed from the engine compartment bay. All lines were found secure with consistent evidence of safety wire usage. The electrical connection at the fuel pressure-warning switch was found secure. The Intake Guide Vane Ram Assembly (IGV) was secure. Inspection of the air inlet showed damage to the IGV plus first and second stage compressors. The IGV showed FOD damage to the vane leading edge as well as the vane chord, pressure side. Several of the first and second stage compressor blades showed FOD damage to the leading edges, predominately mid-length to tip. The engine would not turn by hand.

A partial engine disassembly was then conducted in an attempt to locate the source of the mechanical lockup. Three of the eight combustion chambers were removed and inspected. All of the chambers contained moderate concentrations of metallizing (splatter) affixed to the chamber walls adjacent to the fuel nozzle ejector exit. Small flakes of a silver material were noted lying loose in the chamber. After removal of the combustion chambers, the leading edges of the HP Turbine was noted to contain heavy concentrations of a brittle black deposit formed around the blades. With the combustion chambers removed, the compressor outlet from the 12th stage could be viewed. Several broken ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX00LA034