N550RT

Substantial
None

Beech 95-B55 S/N: TC-2101

Accident Details

Date
Friday, November 19, 1999
NTSB Number
LAX00LA036
Location
PETALUMA, CA
Event ID
20001212X20122
Coordinates
38.209823, -122.760253
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the pilot to maintain adequate airspeed which resulted in a stall/mush condition and subsequent hard landing.

Aircraft Information

Registration
N550RT
Make
BEECH
Serial Number
TC-2101
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
95-B55 BE55
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
KEITH RICHARD E
Address
90 DEER HOLLOW RD
Status
Deregistered
City
ANSELMO
State / Zip Code
CA 94960
Country
United States

Analysis

On November 18, 1999, at 1640 hours Pacific standard time, a Beech 95-B55, N550RT, landed hard and bounced several times before running off the end of the runway at the Petaluma Municipal Airport, Petaluma, California. The airplane, owned and operated by the pilot, sustained substantial damage. The commercial pilot and passenger were not injured. The local area personal flight, conducted under the provisions of 14 CFR Part 91, had originated at the Santa Rosa, California, airport, at 1615, and was en route to Petaluma. Visual meteorological conditions prevailed and no flight plan was filed.

The pilot reported that he was attempting to perform a short field landing to runway 11. He stated that he allowed the airspeed to dissipate too soon and the airplane dropped to the runway and bounced twice before he was able to recover. The stall-warning indicator had not enunciated. The propeller blades and engine mounts were bent and the wings had separated from the fuselage.

The pilot reported that he had not experienced any mechanical problems with the aircraft prior to the accident. He stated that the accident could have been prevented by maintaining "greater speed."

A Federal Aviation Administration (FAA) inspector from the Oakland Flight Standards District Office inspected the aircraft after the accident. He tested the stall indicator warning system and reported that it functioned normally.

The aircraft was equipped with vortex generators. The supplemental type certificate (STC) and the micro vortex generator kit installation manual were reviewed. The kit consisted of 106 vortex generators mounted on the wings, just aft of the boot line and on both sides of the rudder, plus two strakes on the outside of the engine nacelles. The manufacturer reported that the vortex generators had been shown "to substantially reduce stall speeds and Vmca, and to improve stall characteristics." However, they further stated that no flight manual supplement was developed for this specific STC (#SA5789NM), therefore, the original speeds, limitations, and performance data listed in the pilot's operating handbook (POH) were to be used in order to provide an increased margin of safety.

The pilot reported that he used the vortex generator manufacturer's (reduced) speeds he obtained from a sales brochure as his reference airspeeds during the approach, instead of the airspeeds indicated in the POH.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX00LA036