Accident Details
Probable Cause and Findings
A loss of airplane pitch control resulting from the in-flight failure of the horizontal stabilizer trim system jackscrew assembly's acme nut threads. The thread failure was caused by excessive wear resulting from Alaska Airlines' insufficient lubrication of the jackscrew assembly. Contributing to the accident were Alaska Airlines' extended lubrication interval and the Federal Aviation Administration's (FAA) approval of that extension, which increased the likelihood that a missed or inadequate lubrication would result in excessive wear of the acme nut threads, and Alaska Airlines' extended end play check interval and the FAA's approval of that extension, which allowed the excessive wear of the acme nut threads to progress to failure without the opportunity for detection. Also contributing to the accident was the absence on the McDonnell Douglas MD-80 of a fail-safe mechanism to prevent the catastrophic effects of total acme nut thread loss.
Aircraft Information
Registered Owner (Historical)
Analysis
The Safety Board's full report is available at www.ntsb.gov/publictn/publictn.htm.
On January 31, 2000, about 1621 Pacific standard time, Alaska Airlines, Inc., flight 261, a McDonnell Douglas MD-83 (MD-83), N963AS, crashed into the Pacific Ocean about 2.7 miles north of Anacapa Island, California. The 2 pilots, 3 cabin crewmembers, and 83 passengers on board were killed, and the airplane was destroyed by impact forces. Flight 261 was operating as a scheduled international passenger flight under the provisions of 14 Code of Federal Regulations Part 121 from Lic Gustavo Diaz Ordaz International Airport (PVR), Puerto Vallarta, Mexico, to Seattle?Tacoma International Airport (SEA), Seattle, Washington, with an intermediate stop planned at San Francisco International Airport (SFO), San Francisco, California. Visual meteorological conditions prevailed for the flight, which operated on an instrument flight rules flight plan.
The accident airplane arrived at PVR about 1239 on the day of the accident. The inbound pilots stated that they met the accident pilots outside the airplane and briefly discussed its status.
Flight data recorder (FDR) information from the accident flight indicated that during taxi for takeoff, when the FDR started recording, the horizontal stabilizer was at the 7° airplane-nose-up position, which was the takeoff pitch trim setting. About 1337, the accident airplane departed PVR as flight 261. A National Transportation Safety Board review of FAA air traffic control (ATC) tapes and FDR data from the accident flight indicated that the first officer was the pilot flying immediately after the airplane's departure. The flight plan indicated that flight 261's cruising altitude would be flight level (FL) 310.
FDR data indicated that during the initial portion of the climb, the horizontal stabilizer moved at the primary trim motor rate of 1/3º per second from 7º to 2º airplane nose up. According to FDR data, the autopilot was engaged at 1340:12, as the airplane climbed through an altitude of approximately 6,200 feet. Thereafter, the FDR recorded horizontal stabilizer movement at the alternate trim motor rate of 1/10º per second from 2° airplane nose up to 0.4° airplane nose down. At 1349:51, as the airplane continued to climb through approximately 23,400 feet at 331 knots indicated airspeed (KIAS), the cockpit voice recorder (CVR) recorded the horizontal stabilizer move from 0.25° to 0.4° airplane nose down. This was the last horizontal stabilizer movement recorded until the airplane's initial dive about 2 hours and 20 minutes later. At 1353:12, when the airplane was climbing through 28,557 feet at 296 KIAS, the autopilot disengaged.
FDR information and airplane performance calculations indicated that, during the next 7 minutes, the airplane continued to climb at a much slower rate. During this part of the ascent, the elevators were deflected between -1° and ?3°, and the airplane was flown manually using up to as much as 50 pounds of control column pulling force. After reaching level flight, the airplane was flown for about 24 minutes using approximately 30 pounds of pulling force at approximately 31,050 feet and 280 KIAS. The airspeed was then increased to 301 KIAS, and the airplane was flown for almost another 1 hour 22 minutes using about 10 pounds of pulling force. At 1546:59, the autopilot was re?engaged.
According to Alaska Airlines documents, ATC and CVR information, and postaccident interviews with Alaska Airlines dispatch and maintenance personnel, the flight crew contacted the airline's dispatch and maintenance control facilities in SEA some time before the beginning of the CVR transcript at 1549:49 to discuss a jammed horizontal stabilizer and a possible diversion to Los Angeles International Airport (LAX), Los Angeles, California. These discussions were conducted on a shared company radio frequency between Alaska Airlines' dispatch and maintenance facilities at SEA and its operations and maintenance facilities at LAX.
At 1549:56, the autopilot was disengaged; it was re-engaged at 1550:15. According to the CVR transcript, at 1550:44, SEA maintenance asked the flight crew, "understand you're requesting…diversion to LA…is there a specific reason you prefer LA over San Francisco?" The captain replied, "well a lotta times its windy and rainy and wet in San Francisco and uh, it seemed to me that a dry runway…where the wind is usually right down the runway seemed a little more reasonable."
At 1552:02, an SEA dispatcher provided the flight crew with the current SFO weather (wind was 180° at 6 knots; visibility was 9 miles). The SEA dispatcher added, "if uh you want to land at LA of course for safety reasons we will do that…we'll…tell you though that if we land in LA…we'll be looking at probably an hour to an hour and a half we have a major flow program going right now." At 1552:41, the captain replied, "I really didn't want to hear about the flow being the reason you're calling us cause I'm concerned about overflying suitable airports." At 1553:28, the captain discussed with the first officer potential landing runways at SFO, stating, "one eight zero at six…so that's runway one six what we need is runway one nine, and they're not landing runway one nine." The first officer replied, "I don't think so." At 1553:46, the captain asked SEA dispatch if they could "get some support" or "any ideas" from an instructor to troubleshoot the problem; he received no response. At 1555:00, the captain commented, "it just blows me away they think we're gonna land, they're gonna fix it, now they're worried about the flow, I'm sorry this airplane's [not] gonna go anywhere for a while…so you know." A flight attendant replied, "so they're trying to put the pressure on you," the captain stated, "well, no, yea."
At 1556:08, the SEA dispatcher informed the flight crew that, according to the SFO automatic terminal information service, the landing runways in use at SFO were 28R and 28L and that "it hasn't rained there in hours so I'm looking at…probably a dry runway." At 1556:26, the captain stated that he was waiting for a requested center of gravity (CG) update (for landing), and then he requested information on wind conditions at LAX. At 1556:50, the SEA dispatcher replied that the wind at LAX was 260° at 9 knots.
Nine seconds later, the captain, comparing SFO and LAX wind conditions, told the SEA dispatcher, "versus a direct crosswind which is effectively no change in groundspeed…I gotta tell you, when I look at it from a safety point I think that something that lowers my groundspeed makes sense." The SEA dispatcher replied, "that'll mean LAX then for you." He then asked the captain to provide LAX operations with the information needed to recompute the airplane's CG because "they can probably whip out that CG for you real quick." At 1558:15, the captain told the SEA dispatcher, "we're goin to LAX we're gonna stay up here and burn a little more gas get all our ducks in a row, and then we'll uh be talking to LAX when we start down to go in there." At 1558:45, the captain asked LAX operations if it could "compute [the airplane's] current CG based on the information we had at takeoff."
At 1602:33, the captain asked LAX operations for wind information at SFO. LAX operations replied that the winds at SFO were 170° at 6 knots. The captain replied, "that's what I needed. We are comin in to see you." At 1603:56, the first officer began giving LAX operations the information it needed to recompute the airplane's CG for landing.
At 1607:54, a mechanic at Alaska Airlines' LAX maintenance facility contacted the flight crew on the company radio frequency and asked, "are you [the] guys with the uh, horizontal [stabilizer] situation?" The captain replied, "affirmative," and the mechanic, referring to the stabilizer's primary trim system, asked, "did you try the suitcase handles and the pickle switches?" At 1608:03, the captain replied, "yea we tried everything together." At 1608:08, the captain added, "we've run just about everything if you've got any hidden circuit breakers we'd love to know about 'em." The mechanic stated that he would "look at the uh circuit breaker uh guide just as a double check." The LAX mechanic then asked the flight crew about the status of the alternate trim system, and, at 1608:35, the captain replied that "it appears to be jammed…the whole thing, it [the AC load meter] spikes out when we use the primary, we get AC [electrical] load that tells me the motor's tryin to run but the brake won't move it. when we use the alternate, nothing happens."
At 1608:50, the LAX mechanic asked, "you say you get a spike…on the meter up there in the cockpit when you uh try to move it with the…primary right?" According to the CVR transcript, at 1608:59, the captain addressed the first officer before responding to the mechanic, stating, "I'm gonna click it off you got it." One second later, the first officer replied, "ok." At 1609:01, the captain reiterated to the LAX mechanic that the spike occurred "when we do the primary trim but there's no appreciable uh change in the uh electrical uh when we do the alternate." The LAX mechanic replied that he would see them when they arrived at the LAX maintenance facility.
At 1609:13, the captain stated, "lets do that." At 1609:14.8, the CVR recorded the sound of a click and, at the same time, the captain stating, "this'll click it off." According to FDR data, the autopilot was disengaged at 1609:16. At the same time, the CVR recorded the sound of a clunk, followed by two faint thumps in short succession at 1609:16.9. The CVR recorded a sound similar to the horizontal stabilizer-in-motion tone at 1609:17. At 1609:19.6, the CVR again recorded a sound similar to the horizontal stabilizer-in-motion tone, followed by the captain's comment, "you got it?" (FDR data indicated that during the 3 to 4 seconds after the autopilot was disengaged, the horizontal stabilizer moved from 0.4° to a reco...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DCA00MA023