N2832W

Substantial
None

Siai-Marchetti S.205/22R S/N: 4-189

Accident Details

Date
Tuesday, March 14, 2000
NTSB Number
FTW00LA096
Location
RAYVILLE, LA
Event ID
20001212X20630
Coordinates
32.469966, -91.750053
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power for an undetermined reason, which resulted in a forced landing. A factor was the dark night light condition.

Aircraft Information

Registration
Make
SIAI-MARCHETTI
Serial Number
4-189
Engine Type
Reciprocating
Year Built
1969
Model / ICAO
S.205/22R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
S.205/22R

Registered Owner (Current)

Name
IBRAHIM PHILLIP
Address
124 COUNTRY CLUB DR
City
WHITINSVILLE
State / Zip Code
MA 01588-2379
Country
United States

Analysis

On March 13, 2000, at 2330 central standard time, a Siai-Marchetti S.205/22R airplane, was substantially damaged during a forced landing following a loss of engine power near Rayville, Louisiana. The airplane was registered to and operated by the instrument rated private pilot, sole occupant, who was not injured. Dark night visual meteorological conditions prevailed for the 14 Code of Federal Regulations Part 91 personal flight, for which an IFR flight plan was filed. The cross-country flight originated from the Montgomery Regional Airport, Montgomery, Alabama, and was destined for the Shreveport Regional Airport, Shreveport, Louisiana.

According to the pilot, the airplane was flying level at 6,000 feet agl. when he felt an "extreme vibration," followed by a partial loss of engine power, and subsequently, oil appeared on the front windscreen. The pilot declared an emergency to the Fort Worth Air Route Traffic Control Center and was provided radar vectors to the John H. Hooks Jr. Memorial Airport, Rayville, Louisiana. The airplane was descending through 4,000 feet when the pilot observed "sparks" coming from beneath the engine cowling. At 1,300 feet the pilot moved the mixture control to the idle/cut-off position and secured the engine. The airplane touched down short of the runway, struck a fence, and came to a stop upright. The pilot added that during the preflight examination, prior to the accident flight, he confirmed that the engine oil level was normal.

An FAA inspector examined the airplane and stated that the right wing spar was structurally damaged. A review of the airplane's airframe and engine maintenance records revealed that the airframe had accumulated a total of 1,940.0 hours at the time of the accident and underwent its most recent annual inspection on March 8, 2000. The airplane was equipped with a 220-horsepower Franklin 6A-350-CIR engine. The engine had accumulated a total of 240.6 hours since major overhaul at the time of the accident, and underwent its most recent 100-hour inspection on March 8, 2000, 15.8 hours prior to the accident. A review of the maintenance records did not reveal evidence of any uncorrected maintenance discrerpancies. The reason for the loss of engine power was not determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW00LA096