N10100

Substantial
None

Piper PA-18-150 S/N: 18-8481

Accident Details

Date
Tuesday, April 18, 2000
NTSB Number
ANC00LA048
Location
BIG LAKE, AK
Event ID
20001212X20753
Coordinates
61.460517, -150.089355
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's excessive application of heel brakes. A factor associated with this accident was the pilot's lack of experience in the make and model of airplane.

Aircraft Information

Registration
N10100
Make
PIPER
Serial Number
18-8481
Engine Type
Reciprocating
Model / ICAO
PA-18-150 PA18
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BOEING CO
Address
VERTOL DIVISION
100 WOODLAND AVE
Status
Deregistered
City
MORTON
State / Zip Code
PA 19102
Country
United States

Analysis

On April 18, 2000, at 1500 Alaska daylight time, a tundra tire equipped Piper PA-18-150 airplane, N10100, sustained substantial damage when it nosed over during taxi for takeoff at the Goose Bay Airport, Big Lake, Alaska. The solo airline transport pilot was not injured. The airplane was owned by the pilot and operated under 14 CFR Part 91. The personal flight departed the Lake Hood Airstrip, Anchorage, Alaska, about 1430 for Goose Bay to practice landings. Visual meteorological conditions prevailed at the time of the accident, and no flight plan was filed.

The pilot told the NTSB investigator-in-charge, during an interview on April 19, that he was taxiing for takeoff in the newly purchased airplane. He indicated that when he applied the heel brakes, the airplane nosed over.

He wrote in his NTSB Pilot/Operator report that this was his first flight in the airplane without the weight of another person in the back seat. He added that the airplane was modified with a nose mounted battery, double puck brakes, and a boosted brake system. He felt that the forward center of gravity and strong brake system, led the airplane to be prone to nose over with excessive braking. He said he was unfamiliar with the newly purchased aircraft, and did not compensate for this tendency.

Inspection of the airplane by an FAA airworthiness inspector, after the airplane had been turned onto its wheels, revealed damage to both front lift struts, the windshield, the empennage, and the vertical stabilizer. According to the pilot, the initial damage to the airplane consisted of propeller, spinner, cowl, windshield, and the top of the rudder. According to the pilot's written statement, during attempts to turn the airplane over, it fell from near vertical onto its back a second time, resulting in additional damage to the skylight, rudder, fuselage longerons, and lift struts.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC00LA048