N10GX

Destroyed
Serious

Geiling SONERAI II S/N: DG1

Accident Details

Date
Tuesday, May 30, 2000
NTSB Number
FTW00LA164
Location
VICTORIA, TX
Event ID
20001212X21006
Coordinates
28.820304, -96.979888
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The failure of the pilot to maintain airspeed during the takeoff initial climb, which resulted in a stall.

Aircraft Information

Registration
N10GX
Make
GEILING
Serial Number
DG1
Engine Type
Reciprocating
Year Built
1983
Model / ICAO
SONERAI II SBM3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
JORGENSEN CLYDE R
Address
146 WOOD DUCK CT
Status
Deregistered
City
VICTORIA
State / Zip Code
TX 77905-0682
Country
United States

Analysis

On May 30, 2000, at 1500 central daylight time, a Geiling Sonerai II amateur-built experimental airplane, N10GX, was destroyed when it impacted the ground following a loss of control during the initial takeoff climb from the Victoria Regional Airport, near Victoria, Texas. The private pilot, who was the registered owner and operator of the airplane, was seriously injured. Visual meteorological conditions prevailed for the 14 Code of Federal Regulations Part 91 personal flight, and a flight plan was not filed. The local flight was originating at the time of the accident.

According to a witness, the airplane departed from runway 12R. The airplane climbed to 100 feet agl, pitched nose-up, and made a "short right turn to downwind. The aircraft then stalled, the nose descended to a very low attitude and the aircraft impacted the ground." The witness added that "the engine appeared to be running normally and developing enough power" prior to the accident.

Another witness reported that he observed the airplane climbing as it was entering a turn toward the south-southwest. The airplane's "right wing dropped violently as if it stalled and entered into a spin." Subsequently, the airplane impacted the ground.

An FAA inspector, who examined the airplane at the accident site, reported that the fuselage forward of the front seat separated from the airframe and was destroyed by impact forces. He added that the right wing separated from the airframe and the left wing was bent aft.

Multiple attempts to obtain a completed Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) from the pilot were unsuccessful.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW00LA164