N6GE

Substantial
Minor

Eaton ACRO SPORT I S/N: 1

Accident Details

Date
Monday, June 5, 2000
NTSB Number
CHI00LA153
Location
MALDEN, MO
Event ID
20001212X21173
Coordinates
36.580848, -89.969261
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the water contamination of the fuel system and the inadequate preflight of the airplane by the pilot. The inoperative fuel system drain was a contributing factor. The wheat was a contributing factor.

Aircraft Information

Registration
Make
EATON
Serial Number
1
Engine Type
Reciprocating
Model / ICAO
ACRO SPORT I SBM3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
ACRO SPORT I

Registered Owner (Current)

Name
LEMONS CHRISTOPHER P
Address
15333 COUNTY ROAD 413
City
DEXTER
State / Zip Code
MO 63841-9056
Country
United States

Analysis

On June 5, 2000, at 0905 central daylight time, an Eaton Acro Sport I, N6GE, owned and operated by the pilot, was substantially damaged during a landing attempt on runway 36 (5,011 feet by 100 feet, asphalt) at the Malden Municipal Airport (MAW), Malden, Missouri. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The commercial pilot reported minor injuries. The local flight departed the Dexter Municipal Airport, Dexter, Missouri, at 0845.

The pilot reported the following in a written statement, "...Approximately 15 minutes into the flight the engine began to sputter out and then suddenly quit. I switched tanks and pumped the manual "wobble" pump, the engine restarted and I gained some altitude. The engine was still running rough so I tried to make it to the nearest airport. (MAW) The engine quit and restarted several more times and finally quit completely just as I turned to try to make the runway. I ended up having to attempt landing short of the runway in a wheat field. The wheels bogged down in the wheat and I nosed over."

The pilot also reported that the quick drain valve was not functioning properly.

A mechanic inspected the airplane and reported finding water in the airplane's fuel system.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI00LA153