N649HA

Substantial
Minor

McDonnell Douglas DC-9-51S/N: 47715

Accident Details

Date
Thursday, June 15, 2000
NTSB Number
LAX00FA229
Location
Lihue, Kauai, HI
Event ID
20001212X21253
Coordinates
21.976110, -159.338882
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
137
Total Aboard
139

Probable Cause and Findings

The first officer's delayed and misjudged landing flare resulting in a tail strike and hard landing. Contributing factors were his relative inexperience flying the type of airplane, and the captain's and the first officer's failure to adhere to required company procedures and Federal Aviation Regulations.

Aircraft Information

Registration
N649HA
Make
MCDONNELL DOUGLAS
Serial Number
47715
Year Built
1976
Model / ICAO
DC-9-51

Registered Owner (Historical)

Name
SALE REPORTED
Address
720 KINDLEBERGER RD
Status
Deregistered
City
KANSAS CITY
State / Zip Code
KS 66115-1115
Country
United States

Analysis

HISTORY OF FLIGHT

On June 14, 2000, about 1710 Hawaiian standard time, a McDonnell Douglas DC-9-51, N649HA, operated by Hawaiian Airlines, Inc., as flight number 193, made a hard landing, striking its tail, on runway 35 at the Lihue Airport, Lihue, Hawaii. The airplane was substantially damaged. There were a total of 139 persons on board the airplane. Neither the airline transport certificated captain, the first officer, nor the three flight attendants were injured. Two of the 134 passengers received minor injuries. The flight was being performed under 14 CFR Part 121. Daytime visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed. The flight originated from Honolulu, Hawaii, about 1643, as a nonstop domestic passenger flight to Lihue. The flight's scheduled arrival time at Lihue was 1635.

The captain reported, that on the day of the accident, he and the first officer were scheduled to fly three round trips to Lihue and a round trip to Kona, Hawaii. The captain flew the first flight to Lihue, and the first officer flew back to Honolulu. The captain indicated that the first officer "made a good landing in Honolulu." On the second flight to Lihue (the accident flight), the first officer was at the controls. The flight departed from Honolulu about 40 minutes behind schedule. The captain further reported that the takeoff, en route, and approach portions of the flight were normal. No evidence of any mechanical malfunction or flight control anomalies was noted during the flight. During the approach to Lihue, the first officer made "appropriate corrections" to maintain the glide slope.

Approaching the airport, at 1702:31, the captain received an air traffic control clearance to perform a VOR/DME runway 35 instrument approach. At 1704:31, the crew reported having the field in sight, and at 1705:48, the airplane was cleared to land.

In Hawaiian Airline's (the operator's) completed "Aircraft Accident Report," the operator indicated that the initial approach was conducted in accordance with the standards established in the approved "Flight Crew Operating Manual," including a Vref of 127 KIAS and use of the instrument landing system/precision approach path indicator (ILS/PAPI) as backup. The applicable crosswind corrections were applied. The final approach segment was commenced with stabilized engine thrust and with a stabilized rate of descent. The captain performed the duties of safety pilot, completing checklists, acknowledging tower instructions, and making required call-outs.

The operator additionally reported that the approach terminated in a "higher-than-normal, although not excessive," deck angle, and an abnormally high rate of sink from 50 feet above ground level to touchdown. The resulting hard landing caused portions of the aft fuselage to come in contact with the runway.

According to the captain, the landing was firmer than routine but he would not consider it to have been a "hard landing." A Hawaiian Airlines flight attendant occupied the fourth flight attendant jump seat because the airplane was completely full. The flight attendant reported that the flight seemed normal until the "hard landing" occurred, which really shook him up. He was "alarmed by the loud sound of metal impacting the ground," and the seat belt shoulder harness kept him from becoming airborne. Several oxygen compartments opened resulting in oxygen masks hanging from the ceiling. The flight attendant then disembarked from the tailcone stairway exit. Upon looking at the outside airplane structure, the attendant "noticed the safety skid plate device (was) badly scraped and around the panel, liquid (was) dripping."

In preparation for their next flight, the captain performed a walk around visual inspection of the airplane. The captain reported that the "tail bumper compression indicator was safety wired and in its normal position." Thereafter, passengers boarded the airplane and they flew to Honolulu. The captain additionally reported that at Honolulu he "called maintenance out as a prudent matter of practice." He explained to the mechanics that the first officer had landed "firmer than routine," and he asked the mechanics to inspect the airplane and to paint the tail bumper if needed. The captain also reported that he did not enter a write-up in the logbook, "as there was no damage to the airplane and the tail bumper indicator pin was up, safetied and in its normal position in Honolulu as it was in Lihue."

The first officer similarly reported that he had performed a walk around inspection of the airplane following his firm landing, and no obvious damage was noted. The last four flights for the day in the airplane were routine.

PERSONNEL INFORMATION

Captain.

The captain possessed an airline transport pilot certificate and had approximately 11,725 hours total flight time. He possessed a type rating in the DC-9, and had about 6,678 hours of flying time as captain in the airplane. During the preceding 90 and 30 days, he had flown the airplane for 240 and 63 hours, respectively. The captain was not a designated check airman in the DC-9.

First Officer.

The first officer possessed an airline transport pilot certificate, and he had approximately 8,895 hours total flight time. He was not type rated in the DC-9. His total time flying the DC-9 was 61 hours, which was all obtained within 90 days of the accident flight. The first officer was type rated in the Embraer EMB-110.

Hawaiian Airline's Director of Flight Safety and Compliance reported to the National Transportation Safety Board investigator that the company had evaluated the first officer throughout his training. The company opined that, by the conclusion of his required training, the pilot's performance had met the minimum acceptable standards to be released for line flying. The company noted, however, that the pilot's performance had been problematic. He had required about twice the number of hours in training, including landing practice, than the average pilot undergoing initial operating experience (IOE) training. The first officer satisfactorily completed the IOE line check in the DC-9 on June 9, 2000.

AIRCRAFT INFORMATION

The airplane was manufactured in 1976. By the accident date, its airframe's total time was about 43,780.23 hours. The airplane had 64,951 total cycles.

The operator's management personnel reported that the airplane's weight and balance were within prescribed limits during the accident flight. The airplane's maintenance log indicated that the number one (left) thrust reverser was inoperative and maintenance action was deferred in accordance with the Hawaiian Airlines DC-9 approved minimum equipment list. The cockpit was accordingly placarded. The flight crew had operated the airplane in this condition on three previous legs.

As described in the airplane's "Flight Crew Operating Manual" and related publications, the DC-9 is equipped with a tail bumper compression indicator. The indicator is attached to the bumper assembly by a hinge, and it is located next to a skid assembly, which is connected to a pneumatic strut in the aft belly of the airplane. The tail bumper compression indicator should normally be in the horizontal position. If the tail bumper has contacted the ground and has been compressed 3 inches or more, the indicator will be driven toward the vertical position. In this event a structural inspection of the airframe is necessary. If the indicator is not in the normal horizontal position, a visual check for damage to the tail bumper skid should be made.

METEOROLOGICAL INFORMATION

About 1655, Lihue's automatic terminal information service reported "Information Alpha" was in effect. In part, it stated that the weather was as follows: "wind zero seven zero at niner visibility one zero few clouds at four thousand five hundred temperature two seven dew point two one altimeter three zero zero one vor dme three five and visual approach in use...."

About 1706, the pilot was advised that Lihue's local wind was from 070 degrees at 8 knots.

AIDS TO NAVIGATION

According to Federal Aviation Administration (FAA) records of facility operations, all electronic aids to navigation pertinent to the airplane's approach and landing were functional on the day of the accident. No anomalies were reported.

AIRPORT AND GROUND FACILITIES

Lihue's runway 35 is 6,500 feet long by 150 feet wide. It has a grooved asphalt surface. The runway is equipped with a (PAPI) visual glideslope indicator system.

Hawaiian Airlines designated the Lihue Airport as being a "special airport," in accordance with federal aviation regulations.

FLIGHT RECORDERS

The Safety Board's Office of Research and Engineering, Washington, D.C., performed a study of the airplane's track to the Lihue Airport using recorded radar data. In summary, the study indicates that from a point about 3 miles south of the airport, to landing, the airplane tracked directly inbound following the runway's centerline extension. A comparison between a 3-degree glideslope and the airplane's descent profile indicated that the airplane's descent track was nearly consistent with the glideslope profile during the airplane's last 1 minute and 1 mile of flight. Some altitude variations were noted, as indicated in the study.

The Safety Board's Vehicle Recorders Division Flight Recorder Laboratory performed a readout of the airplane's digital flight data recorder. In summary, the date indicates that about 2 seconds prior to touchdown the airplane's indicated airspeed, pitch angle, and rate of descent were 130 knots, 3.6 degrees, and -437 feet per minute, respectively. About 1 second prior to touchdown the airplane's indicated airspeed, pitch angle, and rate of descent were 127 knots, 5.8 degrees, and -384 feet per minute, respectively.

About the time of touchdown, the airspeed was 126 knots, and the ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX00FA229