N1927Y

Substantial
Minor

Mooney M20E S/N: 234

Accident Details

Date
Wednesday, August 2, 2000
NTSB Number
SEA00LA150
Location
OREGON CITY, OR
Event ID
20001212X21857
Coordinates
45.319442, -122.520271
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A loss of engine power for undetermined reason(s). A factor was the rough/uneven terrain.

Aircraft Information

Registration
N1927Y
Make
MOONEY
Serial Number
234
Engine Type
Reciprocating
Model / ICAO
M20E M20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
FLITEWALLET LLC
Address
1009 COURT ST
Status
Deregistered
City
THE DALLES
State / Zip Code
OR 97058-2219
Country
United States

Analysis

On August 1, 2000, approximately 1830 Pacific daylight time, a Mooney M20E, N1927Y, registered to Wrightco Motorcycle Accessories, Inc., and being flown by a private pilot, was substantially damaged during a forced landing six nautical miles southeast of Oregon City, Oregon. The pilot sustained minor injuries. Visual meteorological conditions existed and no flight plan had been filed. The flight, which was personal, was operated under 14CFR91, and originated from Estacada, Oregon, and was en route to Mulino, Oregon.

The pilot reported in a telephonic interview that he had initiated a descent from 2,000 feet above sea level to his destination when the engine abruptly stopped operating. He then attempted to trouble shoot the power loss by selecting alternate fuel tanks, and then boost pump operation, without success. He then executed a forced landing to an agricultural field encountering rough terrain during the landing rollout.

Post-crash examination and test run of the engine by the Federal Aviation Administration's (FAA) Hillsboro, Oregon, Flight Standards District Office inspector assigned to the accident was conducted shortly after the accident. The aircraft was leveled at the site and both left and right fuel tanks were observed to be approximately half full. The inspector reported that during the test run, the "fuel control servo appeared to be blocked for unknown reason" and that "fuel pressure going in the fuel servo was considerably/extremely low at [the] outlet and would not sustain engine operation."

The fuel servo unit was removed from the aircraft's Lycoming IO-360-A1A engine and shipped to the Safety Board's Northwest Regional Office. It was subsequently flow checked at the facilities of Precision Airmotive on October 20, 2000. No discrepancies were noted during the flow check (refer to attached report).

The fuel servo was returned to the maintenance facility that had removed it with instructions to re-install it in the aircraft. The FAA's Hillsboro Flight Standards District Office inspector assigned to the investigation returned to the maintenance facility and observed a second test run of the engine. He reported that the engine successfully operated with no discrepancies noted.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA00LA150