N68FM

Substantial
Minor

Mooney M20S S/N: 30-0031

Accident Details

Date
Thursday, September 28, 2000
NTSB Number
LAX00LA352
Location
SAN CARLOS, CA
Event ID
20001212X22024
Coordinates
37.490158, -122.260894
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain directional control of the airplane during an aborted landing.

Aircraft Information

Registration
N68FM
Make
MOONEY
Serial Number
30-0031
Engine Type
Reciprocating
Year Built
1999
Model / ICAO
M20S M20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
JCASL LLC
Address
520 S EL CAMINO REAL STE 240
Status
Deregistered
City
SAN MATEO
State / Zip Code
CA 94402-1715
Country
United States

Analysis

On September 27, 2000, at 1820 hours Pacific daylight time, a Mooney M20S, N68FM, was substantially damaged by impact with a hangar during an aborted landing at the San Carlos, California, airport. The private pilot, the sole occupant, received minor injuries. Visual meteorological conditions prevailed for the personal flight that was operated by the owner under 14 CFR Part 91. The flight departed from Prescott, Arizona, at 1445. No flight plan was filed.

According to a Federal Aviation Administration inspector, witnesses reported the pilot's first landing approach to runway 30 was too high and the pilot performed a go-around. The second approach to the same runway was also high and the aircraft touched down and began porpoising. After two bounces, it appeared to witnesses that the pilot attempted another go-around; however, the aircraft drifted off the runway to the left and the left wing struck a hangar in the northwest corner of the airport. The aircraft came to rest between two rows of hangars. There was a postcrash fire.

The pilot reported that he attempted the go-around after several bounces by placing "the power to full, verified mixture rich, and placed the wing flaps in the 10 [degree] position." He said the plane began to veer to the left of the runway and, although he applied right rudder and right aileron, the drift to the left continued. The stall warning horn never sounded prior to the left wingtip hitting the hangar. The pilot also reported there were no mechanical malfunctions with the airplane; however, during the attempted go-around, it didn't feel or sound as if the engine was producing full power.

In a telephone interview with the Safety Board investigator, the pilot stated that the flying day had started in San Antonio, Texas, with a fuel stop in Prescott, and then continuation to San Carlos. The en route flying time was 7.5 hours at 8,500 feet, without supplemental oxygen, and he acknowledged that fatigue might have been a factor in the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX00LA352