Accident Details
Probable Cause and Findings
Total blockage of the instrument static system due to ice.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On October 26, 2000, at 1058 hours Pacific daylight time, a Cessna 340A, N4347C, was destroyed when the aircraft impacted mountainous terrain near Julian, California. The airline transport certificated pilot and the commercial certificated second pilot were fatally injured. Instrument meteorological conditions prevailed for the business flight conducted under 14 CFR Part 91 by Marko Foam Products, Inc., of Corona, California. The aircraft departed from the John Wayne Airport - Orange County, Santa Ana, California, at 1031, destined for Calexico, California, and was operating on an instrument flight plan.
About 2 minutes prior to the loss of radar contact, while en route in instrument flight conditions between the Oceanside VORTAC and the Julian VORTAC (radio navigational aides), the flight was handed off to the Los Angeles Air Route Traffic Control Center. The pilot checked in with the center at 11,000 feet and, a short time later, asked what altitude the center showed him to be at on radar. The controller replied that he was not receiving the airplane's mode C altitude information. The pilot then asked for clearance to climb to VFR conditions on top. He reported ". . . our uh altimeter just went down to uh fifty three hundred." He reported the airplane was in the tops of the clouds and needed to go up about 1,000 feet. The controller cleared the aircraft to climb and maintain VFR conditions on top and, a short time later, radar contact was lost.
PERSONNEL INFORMATION
The pilot was the Charter chief pilot at Lenair Aviation at John Wayne Airport and had about 20,000 hours of flight experience. His first-class medical certificate was issued October 2, 2000.
The chief flight instructor of Lenair said that his company regularly provided pilot services to the owner of the accident aircraft. Because they were providing pilots only, the flight operation was conducted under 14 CFR Part 91. On the day of the accident, Lenair assigned the pilot to fly the aircraft to Calexico to pickup employees of the owner and return them to Corona, California, and then return the airplane to John Wayne airport.
The chief flight instructor also said that the second pilot was neither an employee of Lenair nor an assigned crewmember. He was aboard the aircraft without Lenair's knowledge or consent. The pilot who was assigned the trip had, unbeknownst to Lenair, apparently offered the second pilot the opportunity to "ride along." The second pilot was not affiliated with the aircraft owner.
AIRCRAFT INFORMATION
The previous flight of the aircraft was on October 24, 2000. The pilot who flew that flight reported the aircraft was equipped and certified for flight in instrument meteorological conditions, there were no mechanical discrepancies on the aircraft, and that the model 400 autopilot functioned normally. The aircraft was originally manufactured and equipped for approved flight into known icing conditions; however, the windshield heated plate had been removed. The pilot who flew the previous flight believed the remainder of the de-ice equipment was functional although he hadn't had occasion to use it.
The owner of the aircraft reported that the aircraft was only washed when he specifically instructed the washing service to clean it. It was last washed on October 16, 2000, just before he flew the airplane to Colorado Springs, Colorado, and back. He reported that, on that trip, which cruised at 16,500 feet mean sea level (msl), there were no irregularities in any of the instrumentation, in particular, none in the pitot-static instruments.
The last regular maintenance was an annual inspection on January 19, 2000, when the aircraft's total flying time was 3,181.5 hours. The manager of the maintenance facility, which performed the inspection, said the de-ice boot function would have routinely been tested by external visual and tactile examination during ground run-up. According to the shop work order, "several small splits" in the wing de-ice boots were repaired. Airworthiness directive 96-20-07 relating to pressure testing the combustion chamber of the cabin heater was accomplished.
Two maintenance activities were accomplished in the interim following the inspection up to the time of the accident. On May 4, 2000, the right-hand (copilot) attitude indicator was overhauled and replaced, the de-ice boots were "clean[ed] and dressed," and the cockpit seats were reupholstered. On June 30, 2000, the de-ice boot electrical lead on the number 3 blade of the right-hand propeller was replaced and the de-ice ammeter was removed, overhauled, and replaced at aircraft total flight time of 3,233 hours.
According to the aircraft logbooks, new de-ice boots were installed on the horizontal stabilizer on January 23, 1997.
On December 22, 1999, the altimeters and static system were tested and certified in accordance with FAR 91.411 (FAR part 43, appendix E), and the transponder was tested and certified in accordance with FAR 91.413 (FAR part 43, appendix F). The manager of the repair station that performed the pitot/static and transponder tests reported it is normal practice in the course of the static system test to first slightly pressurize the static system (about 200 feet altitude) and open the static system drains to expel any accumulated moisture.
According to production records, provided by Cessna Aircraft, the airplane was manufactured April 5, 1978, with optional equipment installed for flight in known icing conditions. Cessna drawing 5300960, titled "Kit Installation - Known Icing, Model 340," shows this equipment as heated static ports, an electrically heated windshield panel, surface de-ice boots, and propeller de-ice boots. According to the Cessna Pilot's Operating Handbook for the model 340A aircraft, an electrically heated pitot tube was standard equipment.
Also according to the production records, the aircraft did not come from the factory with flight instrumentation installed on the right-hand (copilot's) instrument panel and, according to the Cessna party representative, this means that aircraft would have been delivered with a single static system. The aircraft was equipped with an EA-401A encoding altimeter on the left-hand (pilot's) instrument panel and did have a standby altimeter installed on the right-hand panel. According to the operator, the right-hand panel instrumentation included an attitude indicator (artificial horizon), directional (heading) gyro instrument, airspeed indicator, altimeter, and rate-of-climb indicator. Entries in the aircraft logbook stated that "standby" directional gyro instrument and airspeed indicators were installed on the right panel on February 18, 1982. An attitude gyro instrument was installed on August 22, 1984.
According to the Cessna Pilot's Operating Handbook, there are three switches on the left side of the cockpit which operate the de-icing equipment; one for surface de-ice (boots), another for "Pitot Heat" and a third for "Stall and Vent Heat." The third switch, "Stall and Vent Heat," when turned on, supplies electrical power to the static vent heaters, the stall vane heaters, and the wing locker fuel tank vent heater. The "Pitot Heat" switch provides electrical power to the pitot tube heater element only. According to the Cessna Aircraft company party representative, the "Pitot Heat" switch and the "Stall and Vent Heat" switch are adjacent to one another on the switch panel. A supplement to the handbook describes the equipment and provides instructions for preflight functional testing of the heaters.
METEOROLOGICAL INFORMATION
The chief flight instructor at Lenair Aviation reported that the pilot obtained a weather briefing and filed an instrument flight plan using Lenair's DUATs weather access computer before going to the aircraft.
According to the Factual Report of the Safety Board's Air Traffic Specialist (see Communications, below), at 0941, the pilot contacted San Diego Automated Flight Service Station (San Diego AFSS) and filed an instrument flight rules (IFR) flight plan departing John Wayne/Orange County, California, airport (SNA) "A S A P." The pilot requested a route via Seal Beach (SLI), Oceanside (OCN), and Julian (JLI) VORs (radio navigational aides), direct to the KUMBA intersection, direct to his destination of Calexico, California (CXL). Requested cruising altitude was 11,000 feet (msl) and estimated time of arrival at CXL was 1847. The flight plan indicated the airplane was equipped with an IFR certified GPS receiver and would cruise at a true airspeed of 200 knots. The pilot then requested a weather briefing. The San Diego AFSS specialist advised the pilot of conditions in the area, read weather observations along the requested route of flight, and said there would be "multiple layers of clouds west of the mountains." The specialist advised the pilot that winds at 11,000 feet were forecast to be "from the southwest, two four zero at twenty two knots," and advised that "the freezing level is also at eleven thousand."
COMMUNICATIONS
A Safety Board Air Traffic Control Specialist examined flight plan, weather, and Air Traffic Control (ATC) communications and automation data obtained from the Federal Aviation Administration (FAA) Los Angeles Air Route Traffic Control Center (Los Angeles Center) and Southern California Terminal Radar Approach Control (SoCal TRACON). Recorded radar data was obtained from Los Angeles Center and SoCal TRACON. Additional recorded search (primary) radar data was obtained from U.S. Air Force 84th Radar Evaluation Squadron (RADES). The Safety Board Specialist's factual report is attached.
According to the Specialist's report, the pilot filed an instrument flight rules (IFR) flight plan from John Wayne/Orange County Airport to his destination at Calexico via the Seal Beach, Oceanside, and Julian VOR navigation aides and thence via KUMBA intersection to Calexico, an...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX01FA026