N972AE

Substantial
None

Eurocopter AS 350B-3 S/N: 3234

Accident Details

Date
Wednesday, November 15, 2000
NTSB Number
LAX01LA042
Location
MESA, AZ
Event ID
20001212X22306
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The dual student's misjudged landing flare and level off, which resulted in a heel first touchdown and subsequent hard landing during a practice autorotation. Also causal was the instructor pilot's inadequate supervision of the student.

Aircraft Information

Registration
Make
EUROCOPTER
Serial Number
3234
Engine Type
Turbo-shaft
Year Built
1999
Model / ICAO
AS 350B-3
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
6
FAA Model
AS 350 B3

Registered Owner (Current)

Name
BANK OF UTAH TRUSTEE
Address
50 S 200 E STE 110
City
SALT LAKE CITY
State / Zip Code
UT 84111-1617
Country
United States

Analysis

On November 15, 2000, at 1030 hours mountain standard time, a Eurocopter AS-350-B3, N972AE, was substantially damaged during a hard landing at Falcon Field, Mesa, Arizona. The airline transport certificated instructor pilot and the certificated commercial pilot under instruction were not injured. No flight plan was filed for the local area instructional flight, which departed from Falcon Field about 1000. The flight was operated under 14 CFR Part 91 by Petroleum Helicopters, Inc. Visual meteorological conditions prevailed.

The pilot reported that he had demonstrated an autorotation landing and then turned control of the helicopter over to the student to perform the next autorotation landing. The student's entry was abrupt resulting in first, high rotor rpm, then low rpm; however, the rpm was proper prior to initiating the landing flare. The student's initial pitch application during the flare was a little too high but okay. As the aircraft neared the landing, additional collective was applied, but it was insufficient to check the sink rate and the heels of the skids made ground contact, rocking the helicopter first forward onto the toe of the skid and then back down on the full skid. The pilot heard a metallic sound and, on external inspection, found the tail boom was bent down.

The pilot noted that a ballast installation in the tail boom might have contributed to the accident. The helicopter was configured for EMS (Emergency Medical Service) use with a stretcher installation. Part of the EMS modification moved the 48-pound battery into the tail cone forward of the stabilizer and installed a ballast station rated for up to 19.22 pounds of lead ballast in the tip of the tail cone. Both the battery relocation and the ballast installation were installed in accordance with an American Eurocopter Supplemental Type Certificate (STC). The accident helicopter was carrying 18.3 pounds of lead ballast in addition to the relocated 48-pound battery.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX01LA042