N94432

Substantial
None

Ercoupe 415GS/N: 5078

Accident Details

Date
Saturday, January 20, 2001
NTSB Number
SEA01LA040
Location
Santiam, OR
Event ID
20010206X00409
Coordinates
44.410530, -121.920158
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The partial blockage of the carburetor main metering jet orifice by contamination of undetermined origin. Factors include a snow-covered runway upon which the pilot executed a forced landing.

Aircraft Information

Registration
Make
ERCOUPE
Serial Number
5078
Engine Type
Reciprocating
Year Built
1950
Model / ICAO
415GERCO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
415-G

Registered Owner (Current)

Name
AEROSPACE TRUST MANAGEMENT LLC TRUSTEE
Address
1013 CENTRE RD STE 403A
City
WILMINGTON
State / Zip Code
DE 19805-1270
Country
United States

Analysis

On January 20, 2001, approximately 1430 Pacific standard time, an Ercoupe 415G, N94432, nosed over in the snow during a forced landing at Santiam Junction State Airport, Santiam, Oregon. The private pilot, who was the sole occupant, was not injured, but the aircraft, which was owned and operated by the pilot, sustained substantial damage. The 14 CFR Part 91 personal pleasure flight, which was en route to Prineville, Oregon, in visual meteorological conditions, departed Independence, Oregon, about 55 minutes earlier. No flight plan had been filed. The ELT, which was activated by the accident sequence, was turned off at the scene.

According to the pilot, just after he passed Santiam Junction Airport, the aircraft's engine began to lose power. He therefore applied carburetor heat and turned back toward the airport. Soon thereafter, the engine went to idle RPM, and the pilot elected to execute a forced landing on runway 06 at the Santiam Junction Airport. Although the touchdown was successful, as the aircraft slowed, it nosed over in the snow that had accumulated on the runway surface. According to the pilot, the snow was approximately two feet deep.

During a post-accident engine examination, the carburetor was disassembled, and it was discovered that the orifice to the main metering jet was almost completely plugged by ball of putty-like contaminant. No similar material was found anywhere else in or on the carburetor, and it could not be determined when or how the contamination had entered the carburetor bowl.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA01LA040