N4823V

Substantial
None

Cessna 172RGS/N: 172RG0391

Accident Details

Date
Saturday, March 24, 2001
NTSB Number
FTW01LA085
Location
Waco, TX
Event ID
20010330X00672
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the failure of the number four cylinder exhaust valve which resulted in a total loss of engine power during cruise. A contributing factor was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
Make
CESSNA
Serial Number
172RG0391
Engine Type
Reciprocating
Year Built
1980
Model / ICAO
172RGC72R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172RG

Registered Owner (Current)

Name
STRATUS AIR LLC
Address
6564 FLEUR DE LIS DR APT 13
City
NEW ORLEANS
State / Zip Code
LA 70124-1455
Country
United States

Analysis

On March 23, 2001, at 1845 central standard time, a Cessna 172RG single-engine airplane, N4823V, was substantially damaged during a forced landing following a loss of engine power near Waco, Texas. The airplane was registered to and operated by the pilot. The commercial pilot and passenger were not injured. Visual meteorological conditions prevailed, and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The cross-country flight originated from the Fort Worth Meacham International Airport, Fort Worth, Texas, at 1800, with a destination of Georgetown, Texas.

The pilot reported that while in cruise flight, at 3,500 feet msl, the engine "began to vibrate excessively and would not produce enough power to maintain altitude." The pilot contacted Gray approach control and requested a heading to the nearest airport. Gray approach control vectored the pilot toward the McGregor Executive Airport near Waco with instructions to turn to a heading of 100 degrees. Approximately 5 miles west of the airport, the engine "quit completely and locked up," and the pilot initiated a forced landing. During the ensuing landing, the airplane touched down in a field, struck a fence and a ditch, nosed over, and came to rest inverted.

Examination of the aircraft by the FAA inspector, who responded to the accident site, revealed that the vertical stabilizer was crushed, the was empennage twisted, and the left wing strut was bent. In addition, the inspector found that the engine's number four cylinder lower spark plug housing was separated from the cylinder.

On April 26, 2001, NTSB investigators and a representative of the engine manufacturer examined the Lycoming O-360-F1A6 (serial number RL-31901-36A) engine at Air Salvage of Dallas, near Lancaster, Texas. Examination of the engine revealed that the number four exhaust valve separated from its stem and was found "wedged" in the spark plug hole. The number four exhaust valve push-rod and push-rod tube were bent aft at the cam follower end. According to the engine maintenance records, the engine was field overhauled on June 22, 1999, and had accumulated approximately 450 flight hours since overhaul at the time of the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW01LA085