N36BJ

Substantial
Serious

Boykin B J B8MS/N: 81679

Accident Details

Date
Friday, April 27, 2001
NTSB Number
FTW01LA114
Location
Clarksville, AR
Event ID
20010503X00863
Coordinates
35.450931, -93.469444
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the pilot's inadequate preflight inspection, which resulted in a loose control stick on takeoff, rendering the aircraft uncontrollable.

Aircraft Information

Registration
N36BJ
Make
BOYKIN B J
Serial Number
81679
Year Built
1979
Model / ICAO
B8M

Registered Owner (Historical)

Name
BOYKIN B J
Address
6 LAKESIDE DR
Status
Deregistered
City
LITTLE ROCK
State / Zip Code
AR 72204
Country
United States

Analysis

On April 27, 2001, at 1030 central daylight time, a Boykin B J B8M, amateur-built experimental gyrocraft, N36BJ, was substantially damaged when it impacted terrain during an uncontrolled descent at the Clarksville Municipal Airport, Clarksville, Arkansas. The gyrocraft was registered to and operated by the pilot. The private pilot, who was the sole occupant, sustained serious injuries. Visual meteorological conditions prevailed and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The local flight departed the Clarksville Municipal Airport at 1000.

According to a written statement provided by the pilot, he had completed 3 touch-and-go landings at the airport. He stated that his 4th takeoff was "normal;" however, as the gyrocraft was climbing through 70 feet, the pilot noticed that the control stick "became difficult to move left and right." The pilot reduced the engine power to idle, and the gyrocraft started to descend to the left. He applied right pressure on the control stick and the control "suddenly became free;" however, "left and right control was lost and the gyrocopter descended to the left." The gyrocraft impacted terrain at 45-50 mph.

In the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2), the pilot stated that the control stick had become "loose." He added under the section titled "Recommendations (How Could This Accident Have Been Prevented)" that he could have conducted "more preflight inspection," and "tighten[ed] all adjuster fittings."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW01LA114