N242KAAllen Rotorway 162F2001-06-03 NTSB Accident Report

Substantial
None

Allen Rotorway 162FS/N: 6307

Summary

On June 03, 2001, a Allen Rotorway 162F (N242KA) was involved in an incident near Jerseyville, IL. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: The improper autorotation by the pilot. Contributing factors were the engine failure for undetermined reason(s) and the muddy terrain.

On June 3, 2001, at 1015 central daylight time, an experimental amateur-built Allen Rotorway 162F, N242KA, sustained substantial damage on impact with terrain following a loss of engine power after takeoff from a farm field near Jerseyville, Illinois. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The private pilot reported no injuries. The local flight was originating at the time of the accident.

In a written statement, the pilot reported "After preflight and startup I allowed the engine to warm up to green arc (mandatory to prevent over pressurization of cooling system).

This incident is documented in NTSB report CHI01LA152. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N242KA.

Accident Details

Date
Sunday, June 3, 2001
NTSB Number
CHI01LA152
Location
Jerseyville, IL
Event ID
20010608X01135
Coordinates
39.109607, -90.320312
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the improper autorotation by the pilot. Contributing factors were the engine failure for undetermined reason(s) and the muddy terrain.

Aircraft Information

Registration
Make
ALLEN
Serial Number
6307
Year Built
1999
Model / ICAO
Rotorway 162F

Registered Owner (Historical)

Name
ALLEN STEVEN H
Address
RR 4 BOX 368
Status
Deregistered
City
JERSEYVILLE
State / Zip Code
IL 62052-9452
Country
United States

Analysis

On June 3, 2001, at 1015 central daylight time, an experimental amateur-built Allen Rotorway 162F, N242KA, sustained substantial damage on impact with terrain following a loss of engine power after takeoff from a farm field near Jerseyville, Illinois. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The private pilot reported no injuries. The local flight was originating at the time of the accident.

In a written statement, the pilot reported "After preflight and startup I allowed the engine to warm up to green arc (mandatory to prevent over pressurization of cooling system). After warmup, all systems in the green I lifted to a hover did a 360 [degree] clearing turn and departed to the south. Approx. 200' AGL 65 mph I noticed the split tach had failed. Almost [immediately] I got a red light indicating No. 1 ECU had failed. I made a 180 [degree] turn back to the pad. At about 100' 40 mph No. 2 ECU failed cutting the engine. Autorotated, [flared] a little late striking tail rotor. Still having forward motion the skids stuck in the mud and the aircraft rolled on to its right side. Shut off all switches and fuel and departed the A/C."

According to the Rotorway 162F pilot operating handbook, a red instrument light annunciation of the electronic control unit (ECU) 1 indicates that the primary ECU is off. Also, flight at 100 feet agl and 40 mph operation is within the shaded area of the height velocity envelope. Referring to the Rotorcraft Flying Handbook (FAA-H-8083-21), the height/velocity (H/V) diagram depicts the critical combination of airspeed and altitude should an engine failure occur. Operating within the shaded area of the H/V diagram may not allow enough time for the critical transition from powered flight to autorotation.

Postaccident examination of the engine by the Federal Aviation Administration (FAA) revealed that the helicopter was fueled with 91-octane automotive fuel. Both electric fuel pumps were operated and fuel was available at the injector ports. The oil screen was checked and reported to be normal. The engine was run at idle and accelerated to 2,600 rpm. After a short period of time, the primary fully automated digital electronic control (FADEC) system was turned off and the secondary FADEC system took control of the engine and it ran normally, but slightly rougher. Both FADEC computer systems were then removed and shipped to Rotorway International, Chandler, Arizona, for inspection and testing.

Inspection and testing of the ECU's, under the supervision of the FAA, revealed that the number one ECU was inoperative and the number two ECU was operational, but it would not communicate with number one ECU. Inspection of the number one ECU's circuit board revealed that the "L1" and "L3" resistors were damaged.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI01LA152