N789MK

Substantial
None

KAINES KITFOX 2S/N: 454

Accident Details

Date
Saturday, June 23, 2001
NTSB Number
CHI01LA185
Location
MT. MORRIS, MI
Event ID
20010628X01284
Coordinates
43.109176, -83.689971
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of partial engine power during takeoff for undetermined reasons. A factor relating to this accident was the tree.

Aircraft Information

Registration
N789MK
Make
KAINES
Serial Number
454
Engine Type
Reciprocating
Model / ICAO
KITFOX 2SA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CIRRUS DESIGN CORP
Address
4515 TAYLOR CIRCLE
Status
Deregistered
City
DULUTH
State / Zip Code
MN 55811
Country
United States

Analysis

On June 23, 2001, at 1803 eastern daylight time, a Kaines Kitfox 2, N789MK, operated by a private pilot, sustained substantial damage when it struck a tree and terrain after taking off from runway 32 (900 feet by 45 feet, grass/turf) at a privately-owned airstrip near Mt. Morris, Michigan. During the takeoff and initial climb, the pilot reported a partial loss of engine power. Visual meteorological conditions prevailed at the time of the accident. The personal flight was being conducted under the provisions of 14 CFR Part 91 without a flight plan. The pilot reported no injuries. The local flight was originating at the time of the accident.

The pilot said that during the takeoff roll, everything seemed to be all right. He said he began to notice that the power was diminishing as he got further down the runway. He said that he was beyond the point where he could safely abort. He got about 30 feet into the air and realized the airplane was not going to sustain flight. The pilot said he decided to put the airplane down in a nearby pasture. During the landing attempt, the airplane's wing struck a tree and then the ground.

The pilot said that both of the airplane's wings were bent aft, the main landing gear were broken aft, and one propeller blade was broken off. Flight control continuity was confirmed. An examination of the engine, engine controls and other airplane systems revealed no anomalies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI01LA185