N9297Z

MINR
Serious

Blanik L-13S/N: 026505

Accident Details

Date
Saturday, August 4, 2001
NTSB Number
CHI01LA277
Location
Marlette, MI
Event ID
20010813X01674
Coordinates
43.319549, -83.080833
Aircraft Damage
MINR
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
1
Total Aboard
2

Probable Cause and Findings

Ground crew personnel improperly connected the tow winch cable prior to takeoff which resulted in one side of the winch cable coming disconnected. Factors associated with the accident were the ditch and the tree branch which the airplane contacted.

Aircraft Information

Registration
N9297Z
Make
BLANIK
Serial Number
026505
Year Built
1975
Model / ICAO
L-13

Registered Owner (Historical)

Name
VULTURES SOARING CLUB INC
Address
590 ROBERTSON CT
Status
Deregistered
City
LAKE ORION
State / Zip Code
MI 48362-2042
Country
United States

Analysis

On August 4, 2001, at 1500 eastern daylight time, a Blanik L-13 glider, N9297Z, collided with a tree during an initial takeoff run at the Marlette Township Airport, Marlette, Michigan. The certified flight instructor (CFI) received a serious injury and the student pilot was not injured. The glider received minor damage. The 14 CFR Part 91 instructional flight was operating in visual meteorological conditions without a flight plan. The local flight was originating when the accident occurred.

The CFI reported, "The slack out - go - signal was given from the operations trailer and take-off power was applied to the winch, whereupon the left hook of the winch harness released, uncommanded, from the center of gravity attachment. The uneven force caused the glider to yaw to the left and head for the ditch on the west side of the runway. I applied right aileron and full right rudder, but was unable to keep the glider from floating into the ditch." The CFI reported the glider ended up bridging the ditch on a heading of east. He reported that the ditch was full of broken and cut down brush and saplings. During the impact, a broken branch penetrated the left side of the cockpit and impaled itself in the CFI's right calf. The CFI remained hospitalized for five days following the accident.

Members of the glider club reported that they had hooked both the left and right side cables prior to the takeoff. Inspection of the tow winch by an inspector from the Federal Aviation Administration Detroit Flight Standards District Office failed to reveal any mechanical failure/malfunction.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI01LA277