N899JG

Substantial
None

John Greenlee X-AircamperS/N: 101

Accident Details

Date
Saturday, August 25, 2001
NTSB Number
FTW01LA199
Location
Healdton, OK
Event ID
20010830X01834
Coordinates
34.230175, -97.486027
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power due to carburetor ice as a result of the pilot's failure to apply carburetor heat during the approach to land. Contributing factors were weather conditions conducive to carburetor icing conditions and the lack of suitable terrain for a forced landing.

Aircraft Information

Registration
Make
JOHN GREENLEE
Serial Number
101
Engine Type
Reciprocating
Year Built
2000
Model / ICAO
X-AircamperBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
PIETENPOL AIR CAMPER

Registered Owner (Current)

Name
GREENLEE MARYANN M
Address
501 E NELSON ST
City
BOWIE
State / Zip Code
TX 76230-3721
Country
United States

Analysis

On August 25, 2001, approximately 0745 central daylight time, a John Greenlee X-Aircamper homebuilt experimental airplane, N899JG, registered to and operated by the pilot, was substantially damaged during a forced landing following a loss of engine power while in the VFR approach pattern to the Healdton Municipal Airport, near Healdton, Oklahoma. The private pilot, who was the sole occupant, was not injured. Visual meteorological conditions prevailed and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The cross-country flight originated from Bowie, Texas, at 0645, and was en route to Healdton, Oklahoma.

According to information provided by the pilot in the enclosed Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2), the pilot was on downwind at Healdton Airport when he experienced a "loss of power." He attempted to "glide" around to the runway, but a "significant south wind complicated the attempt." The airplane cleared trees "by inches and mushed into the ground", about 100-200 feet short of the runway.

The pilot stated that he suspected carburetor ice to have caused the loss of power. According to information on a Carburetor Icing Probability Chart, and the temperature/dewpoint in which the airplane was operating, a "serious icing" probability could have existed.

The vintage airplane was powered by a Ford Model "A" engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW01LA199