N962JA

Substantial
None

Andre Mini Max 1500RS/N: TA962

Accident Details

Date
Monday, September 3, 2001
NTSB Number
NYC01LA220
Location
Chesapeake, VA
Event ID
20010906X01884
Coordinates
36.800735, -76.420394
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to follow the engine manufacturer's descent procedure, which resulted in a lean mixture condition and subsequent engine seizure.

Aircraft Information

Registration
N962JA
Make
ANDRE
Serial Number
TA962
Year Built
2000
Model / ICAO
Mini Max 1500R

Registered Owner (Historical)

Name
ANDRE JOHN D
Address
631 GLADESDALE DR
Status
Deregistered
City
CHESAPEAKE
State / Zip Code
VA 23322-9113
Country
United States

Analysis

On September 3, 2001, about 1315 eastern daylight time, an amateur built Mini Max 1500R, N962JA, was substantially damaged during a forced landing near Chesapeake, Virginia. The certificated private pilot was not injured. Visual meteorological conditions prevailed for the flight that departed a private airport in Saluda, Virginia; destined for Hampton Roads Executive Airport (PVG), Chesapeake, Virginia. No flight plan was filed for the personal flight conducted under 14 CFR Part 91.

The pilot stated that he began a descent from 5,500 feet, toward PVG. During the descent, he maintained a "moderate cruise" power setting, at 5,500 rpm. About 1,500 feet above the ground, the two cycle 2-cylinder Rotax engine lost all power, and the pilot performed a forced landing to a field. During the landing, the airplane struck small trees and sustained substantial damage to the right wing.

The pilot added that the engine experienced a "cold seizure." He believed that the descent at cruise power created a lean fuel/air mixture and subsequent lack of lubrication.

A Federal Aviation Administration inspector examined the airplane. The inspector observed that both pistons exhibited scoring. Photographs of the damaged pistons and cylinders were forwarded to a representative from the engine manufacturer.

According to the manufacturer representative, the failure was directly in line with the exhaust, which was more indicative of a heat seizure, rather than a cold seizure. The representative further stated that a heat seizure was normally associated with excessive exhaust gas temperature, exceeding 1200 degrees F. He assumed that the engine was operating in a lean condition.

An excerpt from the manufacturer's make and model engine manual revealed:

"During cruise and descending it is very important not to create a lean condition with high rpm and low throttle opening. The less fresh charge the engine gets, the more hot residual gas remains in the cylinder. This raises the temperatures to a critical level. For this reason, you may also experience higher exhaust gas and cylinder head temperatures at reduced throttle openings."

Another excerpt from the manual revealed:

"Danger! This engine, by its design, is subject to sudden stoppage! Engine stoppage can result in crash landings. Such crash landings can lead to serious bodily injury or death.

Never fly the aircraft equipped with this engine at locations, airspeeds, altitudes, or other circumstances from which a successful no-power landing cannot be made, after sudden engine stoppage.

Warning! Although these engine types have undergone considerable durability testing, this engine is not a certified aircraft engine. It has not received any individual safety or durability testing and conforms to no aircraft standards. It is for use in experimental and ultralight uncertified aircraft and vehicles only, in which an engine failure will not compromise safety.

User assumes all risk of use and acknowledges by his use the he knows this engine is subject to sudden stoppage."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC01LA220