N3486U

Substantial
None

Cessna 182FS/N: 18254886

Accident Details

Date
Saturday, March 23, 2002
NTSB Number
MIA02LA069
Location
Pell City, AL
Event ID
20020326X00398
Coordinates
33.558887, -86.249443
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's failure to properly recover from a bounced landing resulting in exceedance of the design limits and collapse of the nose gear assembly. A factor in the accident was the pilot's decision to continue flight with a known equipment deficiency.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18254886
Engine Type
Reciprocating
Year Built
1963
Model / ICAO
182FC182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
182F

Registered Owner (Current)

Name
REGISTRATION PENDING
Address
4914 LANE RD
City
ZEPHYRHILLS
State / Zip Code
FL 33541-3506
Country
United States

Analysis

On March 23, 2002, about 1722 central standard time, a Cessna 182F, N3486U, registered to Alabama Skydiving, Inc., operating as a Title 14 CFR Part 91 parachute jump flight, sustained a hard landing and a nose gear collapse at Pell City, Alabama. Visual meteorological conditions prevailed and no flight plan was filed. The airplane sustained substantial damage and the commercially-rated pilot, the sole occupant, was not injured. The flight originated about 10 minutes before the accident.

According to the pilot, prior to the accident flight, the aircraft performed normally in all aspects. Beginning his fourth parachute drop flight of the day, after a takeoff roll of about 3,000 feet and 5 to 10 feet above the 5,002 foot runway, he detected less than normal elevator authority with two parachute jumpers aboard. He decided to continue the takeoff because he had confidence in the power of the engine, and because of the lack of available runway remaining for an abort. Having climbed to release altitude, (3,500 feet, agl) and releasing his jumpers, on return to the field, he decided his best alternative was to use power to control the nose attitude. During his landing flare, he added power to raise the nose and touch down on the main wheels, but the touchdown was hard and the aircraft started a porpoise. The third touchdown was hard enough to collapse the nose gear and cause an excursion off the left side of the runway.

According to an FAA inspector, the pilot stated that he had to ask for help manipulating the yoke in pitch during the takeoff rotation. The inspector examined the flight controls for interference and found none. He found full flight control continuity and authority from stop to stop, and observed no damage to or malfunction of the flight control system.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA02LA069