N46899

Destroyed
Serious

Aeronca O-58BS/N: O58B-4502

Accident Details

Date
Saturday, June 8, 2002
NTSB Number
CHI02LA155
Location
Alexandria, IN
Event ID
20020612X00868
Coordinates
40.232498, -85.633613
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain adequate airspeed which resulted in a stall. A factor was the low altitude.

Aircraft Information

Registration
Make
AERONCA
Serial Number
O58B-4502
Engine Type
Reciprocating
Year Built
1942
Model / ICAO
O-58B
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
0-58B

Registered Owner (Current)

Name
FURLONG KELLY L
Address
20800 TILLMAN MILL RD
City
ATHENS
State / Zip Code
AL 35614-4727
Country
United States

Analysis

On June 8, 2002, at 1211 central daylight time, an Aeronca 0-58B, N46899, piloted by a private pilot, was destroyed during an approach for landing at a private airstrip near Alexandria, Indiana. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 personal flight was not operating on a flight plan. The pilot and passenger were seriously injured. The flight originated from the Huntington Municipal Airport (HHG), Huntington, Indiana, at 1100, en route to Alexandria Airport (I99), Alexandria, Indiana.

In a written statement, the pilot reported that he departed HHG to attend a luncheon at I99. He stated that the accident occurred on landing approach but due to head trauma he received, he was unable to remember specifics or details pertaining to the accident.

In a written statement, the passenger reported that they entered the downwind from runway 27 and saw another airplane on short final. They continued the downwind and noted that another aircraft on the runway appeared that it would need more time to taxi off the runway as there were no taxiways. They continued on the downwind and then made a left hand turn, midfield, to set up for an overhead approach to allow for more spacing between them and the other aircraft which was now on the ground. While initiating the left hand turn, the airplane suddenly got into an unusual attitude. The left wing dipped down and the nose was pointed toward the ground.

The pilot reported in his written statement that there was no mechanical malfunction failure.

The airplane was resting about 20-30 feet to the side of runway 27 with its nose facing north. Ground scaring consisted of the area underlying the airplane. The nose of the airplane exhibited a nose down crush angle with no lateral deformation the airplane's empennage. Examination of the wreckage by the Federal Aviation Administration revealed no mechanical anomalies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI02LA155