N356RB

Substantial
Minor

Brooks Sonerai 2LS/N: 1493

Accident Details

Date
Friday, September 6, 2002
NTSB Number
CHI02LA274
Location
Canton, IL
Event ID
20020909X01563
Coordinates
40.569168, -90.074996
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The partial failure of the ignition system, the induction air leak at the carburetor mounting plate, and the pilot's inadvertant stall during the forced landing. Contributing factors were the crack in the electronic ignition coil, and the improper installation of the carbuetor resulting in an induction air leak.

Aircraft Information

Registration
N356RB
Make
BROOKS
Serial Number
1493
Engine Type
Reciprocating
Model / ICAO
Sonerai 2LSA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
4303 BROOKSIDE DR
Status
Deregistered
City
HEMET
State / Zip Code
CA 92545-8988
Country
United States

Analysis

On September 6, 2002, at 1010 central daylight time, an amateur-built Brooks Sonerai 2L, N356RB, piloted by a commercial pilot, was substantially damaged during a forced landing following a partial loss of engine power immediately after takeoff. The airplane had just departed runway 18 (3,899 feet x 75 feet, asphalt) at the Ingersoll Airport (CTK), Canton, Illinois, with the intention of remaining within the local traffic pattern. Visual meteorological conditions prevailed. The flight was being conducted under 14 CFR Part 91 and was not on a flight plan. The pilot sustained minor injuries.

In his written statement, the pilot noted that shortly after takeoff, approximately 100 feet agl, "the engine began to sputter and lose r.p.m.'s." He reported that he was not able to return to the airport due to the reduction in power available. He selected a bean field, and set up for a forced landing. He stated "I apparently stalled the a/c in an almost wings level condition at maybe 25' a.g.l." The aircraft impacted the bean field, "collapsed the gear, bounced in the air and went over on its tail", according to the pilot.

The pilot reported that he had installed a new carburetor in the days prior to the accident. "The new carb required that I have an adapter piece fabricated to mate to the existing intake manifold flange - which I did." The pilot goes on to state that he had made two static run-ups with no problems noted. In addition, he reported that he had conducted a full static run-up shortly before takeoff on the accident flight.

A post-accident examination revealed that the mounting flanges of the aircraft engine intake manifold and the carburetor mounting flange did not seal completely. In addition, one coil on the electronic ignition was found to be cracked and failed to produce a spark at its associated spark plugs.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI02LA274