N3989H

Substantial
None

Ercoupe (Eng & Research Corp.) 415-CDS/N: 4690

Accident Details

Date
Sunday, September 15, 2002
NTSB Number
CHI02LA281
Location
EFFINGHAM, IL
Event ID
20020917X04182
Coordinates
39.110282, -88.550239
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The partial loss of engine power due to the seized exhaust valve. A factor was the soft field.

Aircraft Information

Registration
Make
ERCOUPE (ENG & RESEARCH CORP.)
Serial Number
4690
Engine Type
Reciprocating
Year Built
1947
Model / ICAO
415-CDERCO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
415-CD

Registered Owner (Current)

Name
ALLEN ARLAN R
Address
4201 W LUKE AVE
City
PHOENIX
State / Zip Code
AZ 85019-2022
Country
United States

Analysis

On September 15, 2002, at 0815 central daylight time, an Ercoupe 415-CD, N3989H, sustained substantial damage when it had a partial loss of engine power after takeoff and nosed over during a forced landing to a cornfield. The commercial pilot and the passenger were not injured. The 14 CFR Part 91 positioning flight was departing from runway 29 (5,100 feet by 75 feet) at the Effingham County Memorial Airport (1H2), Effingham, Illinois. The final destination was Santa Monica, California. Visual meteorological conditions prevailed and no flight plan was filed.

The airplane was purchased on September 13, 2002. The airplane received an annual maintenance inspection on September 13, 2002, prior to the sale of the airplane. The pilot reported that he and the new owner picked the airplane up at Chapin Field (1B8), Cambridge, New York, and intended to fly the airplane to Santa Monica, California. They departed 1B8 and flew to Ithica (ITH), New York, on the first day of the flight. They flew to 1H2 on their second day of the flight. The pilot reported the flights were uneventful.

The pilot reported the following information concerning the accident flight:

"Fueling, preflight, including gas sampling, were normal. Engine start & taxi were normal, however while back taxiing on runway 29, I pulled the Carb. Heat & the engine noticeably ran better. Mag check and run up were normal, minimal differential when carb. heat checked...On take off carb. heat was placed on. The ground run was acceptable & a positive rate of climb was established. At 300 feet +/-, I pushed in the Carb. heat. With no change in engine sound the aircraft began to sink soon after. Prior to touchdown I pulled the power off to minimize engine damage. Landing in a cornfield a few hundred yards from the runway followed...Touch down was on the main landing gear followed by a nose over as the nose wheel dug into the soft dirt."

A Federal Aviation Administration Airworthiness Inspector conducted a post-accident examination of the airplane. He reported that an engine exhaust valve was stuck open.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI02LA281