N440CM

Substantial
None

Charles Maxted RV6S/N: 20539

Accident Details

Date
Monday, September 16, 2002
NTSB Number
MIA02LA169
Location
Bay Minette, AL
Event ID
20020923X05201
Coordinates
30.870277, -87.817497
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The intentional operation of the airplane with known deficiencies with the right magneto resulting in the partial loss of engine power during the initial climb.

Aircraft Information

Registration
N440CM
Make
CHARLES MAXTED
Serial Number
20539
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
RV6RV6
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BRYARS GLENN F
Address
7090 SILVER ST
Status
Deregistered
City
MOBILE
State / Zip Code
AL 36619-1473
Country
United States

Analysis

On September 16, 2002, about 1500 central daylight time, a homebuilt RV6, N440CM, registered to a private individual, experienced collapse of both main landing gears during an aborted takeoff from the Bay Minette Municipal Airport, Bay Minette, Alabama. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight. The airplane was substantially damaged and the private-rated pilot and one passenger were not injured. The flight was originating at the time of the accident.

The pilot stated that during a previous flight, the engine rpm decreased 150 to 175 rpm after switching fuel tanks. He elected to land at the Bay Minette Municipal Airport. While there, 5 gallons of 100 low lead fuel were added and he talked with a mechanic at the airport. He also performed an engine run-up and the engine sounded, "...OK. Not rough as before." He decided to depart intending to climb to 3,000 or 4,000 feet, remaining close to the airport, before deciding to continue to the initial intended destination airport. The engine ran OK until just after liftoff, where the engine began to run rough again. He aborted the takeoff, and landed uneventfully but was unable to stop the airplane on the runway. He intentionally ground looped the airplane to avoid a fence and a 8-foot embankment.

The pilot stated to the Federal Aviation Administration inspector-in-charge (FAA-IIC), that after landing at Bay Minette, he ran the engine which ran rough. Maintenance personnel at Bay Minette advised him that he had a bad right magneto, and repairs could be performed. He (pilot) again ran the engine reporting no magneto drop during the run. He elected to takeoff and continue to his original destination airport.

Following recovery of the airplane, in the presence of the FAA-IIC, the engine was started but could only be operated to between 1,000 and 1,200 rpm due to damage to the engine mount. During the engine run, a magneto check was performed but a rpm decrease could not be detected. Examination of the right magneto revealed that the points were not opening resulting in an inoperative magneto.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA02LA169