N633KF

Substantial
None

Tanner KitfoxS/N: 633

Accident Details

Date
Wednesday, October 2, 2002
NTSB Number
CHI03LA002
Location
Coldwater, MI
Event ID
20021003X05279
Coordinates
41.933612, -85.052780
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The low altitude at which an undetermined loss of engine power occurred following takeoff.

Aircraft Information

Registration
N633KF
Make
TANNER
Serial Number
633
Engine Type
Reciprocating
Year Built
1990
Model / ICAO
KitfoxBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CROOKS JAMES R
Address
6693 US HIGHWAY 79 N
Status
Deregistered
City
DE BERRY
State / Zip Code
TX 75639-3061
Country
United States

Analysis

On October 2, 2002, at 1912 eastern daylight time, an experimental amateur-built Tanner Kitfox, N633KF, was substantially damaged during a forced landing following a takeoff from runway 03 (3,500 feet by 75 feet, asphalt) at Branch County Memorial Airport, Coldwater, Michigan. The airplane experienced a total loss of engine power during climb. Visual meteorological conditions prevailed at time of the accident. The 14 CFR Part 91 instructional flight was not operating on a flight plan. The certified flight instructor (CFI) and pilot were uninjured. The local flight originated at 1800.

The CFI stated that they were performing touch and go's and at 200 feet above ground during the eighth takeoff, there was a total loss of engine power. They then made a left 90-degree turn to a grassy area without attempting to restart the engine. He stated that the airplane impacted at a high sink rate.

Examination of the wreckage was performed by the Federal Aviation Administration. The airplane was resting inverted about 220 feet west of the centerline and 300 feet from the approach end of runway 21. Flight control continuity was confirmed. The fuel shut off valve was in the on position.

The airplane was powered by a Rotax 582LC, serial number 3916612, engine with a total time since overhaul of 232.7 hours and 6 hours were since its last inspection. The engine contained oil and coolant water was present in the coolant tank. Fuel was present in the fuel tank and in both carburetor bowls. The engine was rotated by hand and thumb compression and continuity were confirmed. Electrical continuity of the engine was confirmed upon examination of the ignition system. The spark plugs did not contain debris.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI03LA002