N1955Z

Substantial
None

Wolf Rotorway Exec-162FS/N: 6365

Accident Details

Date
Monday, October 7, 2002
NTSB Number
CHI03LA006
Location
Gregory, MI
Event ID
20021018X05330
Coordinates
42.450000, -84.050003
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Failure of the secondary drive shaft, which resulted in a complete loss of power to the main rotor, and a high forward airspeed on touchdown, causing the helicopter to flip forward.

Aircraft Information

Registration
N1955Z
Make
WOLF
Serial Number
6365
Year Built
2000
Model / ICAO
Rotorway Exec-162F

Registered Owner (Historical)

Name
WOLF J MARK
Address
2855 MASTERS CT
Status
Deregistered
City
PINCKNEY
State / Zip Code
MI 48169-8571
Country
United States

Analysis

On October 7, 2002, approximately 1830 eastern daylight time, an amateur-built Wolf Rotorway Exec-162F helicopter, N1955Z, owned and piloted by a student pilot, was substantially damaged when it lost power to the main rotor and executed an auto-rotation into an open field near Gregory, Michigan. The flight was being conducted under 14 CFR Part 91 and was not on a flight plan. Visual meteorological conditions prevailed at the time of the accident. The pilot reported no injuries. The flight departed the Livingston County Airport (OZW), Howell, Michigan, at 1800 edt for a local flight and was returning to the airport when the accident occurred.

The pilot stated that the "secondary shaft bearing temperature started to rise." He reported that approximately one minute "elapsed from the time the [bearing] temperature increase was noted, to the time the temperature reached 150 degrees Fahrenheit," and the "drive let go", causing the engine RPM to surge. At this point, the pilot noted that all power to the main rotor was lost and he initiated an auto-rotation. He stated that, although the touchdown point was as planned, the forward speed was faster than intended and the helicopter flipped forward and rolled to the left.

Following a post-accident examination, the owner/pilot reported that the secondary drive shaft had failed completely at a point inside the upper bearing race. He noted that the shaft had been in service for approximately 155 hours at the time it failed.

Due to a history of secondary drive shaft failures, Rotorway had released a "re-designed configuration" in April 2001. This configuration increased the shaft diameter from 30 mm to 35 mm. The 30 mm shaft was installed in the accident aircraft.

According to Rotorway, owners were notified of the availability of the new shaft design by an Advisory Bulletin in May 2002. In part, this bulletin states: "The larger [35mm] secondary shaft was supplied with new aircraft and as an upgrade to existing aircraft over a year ago. ... It is the suggestion of Rotorway International that all Rotorway owners consider upgrading to the 35mm secondary shaft." The owner/builder stated that he had planned to upgrade to the 35mm shaft over the coming winter.

In addition, the accident aircraft included an after-market main rotor drive system which incorporated a cog belt in place of the chain drive.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI03LA006