N24BG

Substantial
Serious

Gentry Vari-EzeS/N: 1140

Accident Details

Date
Saturday, October 12, 2002
NTSB Number
SEA03LA002
Location
Shine, WA
Event ID
20021021X05350
Coordinates
47.866390, -122.683334
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Loss of engine power for undetermined reasons during cruise. Trees and objects near the roadway were factors.

Aircraft Information

Registration
N24BG
Make
GENTRY
Serial Number
1140
Engine Type
Reciprocating
Year Built
1980
Model / ICAO
Vari-EzeBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MCCORMACK KENTON J
Address
PO BOX 2015
Status
Deregistered
City
VASHON
State / Zip Code
WA 98070-2015
Country
United States

Analysis

On October 12, 2002, approximately 1200 Pacific daylight time, an experimental Gentry Vari-Eze, N24BG, registered to and operated by the private pilot as a 14 CFR Part 91 personal flight, experienced a loss of engine power and subsequently collided with objects and the terrain near Shine, Washington. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft was substantially damaged and the pilot was seriously injured. The flight departed from Auburn, Washington, at an unknown time and was en route to Port Townsend, Washington.

It was reported that the pilot was flying with a group of other aircraft when he radioed that he was having engine problems. During the forced landing on a rural residential road, the pilot took evasive action to avoid a collision with a vehicle that pulled out onto the road. The aircraft subsequently collided with objects near the road and nosed over, coming to rest inverted.

The wreckage was recovered to Arlington, Washington. On November 8, 2002, investigators from the National Transportation Safety Board and Federal Aviation Administration inspected the engine. The engine remained attached to the firewall. A fuel supply was added and the engine was started. The engine was found to run smooth. Power was increased to 1100 rpm. A magneto check was accomplished with no anomalies noted. Carburetor heat was applied and the engine continued to run smooth for about 5 minutes before it was shut down.

At the time of this writing, the pilot has not responded to the National Transportation Safety Board or completed the Pilot/Operator Aircraft Accident Report Form 6120.1/2.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA03LA002